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ARCHIVED REPORTS_2010_5
EnvironmentalHealth
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4400 - Solid Waste Program
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ARCHIVED REPORTS_2010_5
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Last modified
7/17/2020 8:37:49 PM
Creation date
7/3/2020 10:44:33 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
4400 - Solid Waste Program
File Section
ARCHIVED REPORTS
FileName_PostFix
2010_5
RECORD_ID
PR0440004
PE
4433
FACILITY_ID
FA0004517
FACILITY_NAME
FOOTHILL LANDFILL
STREET_NUMBER
6484
Direction
N
STREET_NAME
WAVERLY
STREET_TYPE
RD
City
LINDEN
Zip
95236
APN
09344002
CURRENT_STATUS
01
SITE_LOCATION
6484 N WAVERLY RD
P_LOCATION
99
P_DISTRICT
004
QC Status
Approved
Scanner
SJGOV\rtan
Supplemental fields
FilePath
\MIGRATIONS\SW\SW_4433_PR0440004_6484 N WAVERLY_2010_5.tif
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EHD - Public
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Vector Engineering, Inc. <br />143E Spring Hill Drive <br />Grass Valley, CA 95945 <br />Telephone: 530-272-2448 <br />Fax: 530-272-8533 <br />Project: LFG Monitoring Well Installation <br />Client: San Joaquin County <br />Location: Foothill Sanitary Landfill <br />6484 North Waverly Road, Linden, CA <br />rn <br />U)J <br />� U � <br />0 a <br />m <br />C7 <br />- <br />121 <br />Page 1 of 1 <br />f <br />Remarks: <br />Moved intermediate plug down 8 ft due to clean sand layer. <br />Shallow probe moved up 1 ft - Probe got stuck in augers <br />during construction and gravel fell in hole before setting pipl. <br />Material Description <br />SP -SM POORLY GRADED SAND WITH SILT (SP-SM)dark brown <br />(7.5YR 3/2), moist, approximately 90 % fine-grained sand, 10 <br />5 % fines <br />10 <br />ML ( SANDY SILT (ML) dark reddish gray (5YR 4/2), moist, <br />15 ( nonplastic, approximately 30 % sand, 70 % fines t <br />20 <br />25 - same, except dark grayish brown (10YR 3/2) 25 <br />30 30 <br />35 I I I I I - increasing sand content, approximately 40 % sand 135 <br />40 L _ 40 <br />SP -SM POORLY GRADED SAND WITH SILT (SP-SMJdark brown <br />(7.5YR 3/2), moist, approximately 90 % fine-grained sand, 10 <br />45 %fines 45 <br />5050 <br />55 ::: SANDSTONE, brown, moderately cemented, fine-grained 55 <br />60 :.. so <br />—------------------------------------- <br />ML SILT (ML), dark brown, moist, approximately 30 % sand, 50 <br />65 % fines, 20 % gravel, pieces of sandstone s5 <br />SP -SM POORLY GRADED SAND WITH SILT (SP-SM)dark brown, <br />70 moist, 80 - 90 % fine-grained sand, 10 - 20 % fines 70 <br />75 75 <br />80 80 <br />85 s5 <br />Well Diagram <br />Bentonite <br />Gravel <br />filter pack <br />Bentonite <br />Gravel <br />filter pack <br />Bentonite <br />Gravel <br />filter pack <br />Drilling Company: Technicon Date Started: 8/3/2009 Time Started: 7:20arn <br />Drilling Method: Hollow Stem Auger Date Completed: 8/3/2009 Time Completed: 3:20pm <br />Boring Diameter: 8 in Elevation (ft): 245.662 Total Depth (ft): 86.5 <br />Logged By: Pete Holland, CEG Groundwater Level: NFWE <br />Sampling Method: Grab from cuttings <br />U] <br />
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