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SECOND QUARTER 2007 GROUNDWATER TREATMENT FACILITY MONITORING REPORT <br /> FORWARD LANDFILL WDR ORDER NO.R5-2003-0080 <br /> with the meteorological station using the telephone line since October 2006. Geo-Logic is <br /> only able to download data by connecting a laptop computer to the station while onsite. <br /> Therefore,it is highly unlikely that the meteorological station is interfering with the GTF <br /> radio transmissions. <br /> As discussed in Section 3.0,the GTF was shut off on May 23,2007,because methylene <br /> chloride and PCE were detected at low concentrations in the effluent sample collected on <br /> May 1, 2007.The GTF was restarted on May 24,2007,and a confirmation effluent sample <br /> was collected on May 25,2007. The GTF was then shut down.VOCs were not detected in <br /> the confirmation effluent sample,and the GTF was restarted for continuous operation on <br /> May 29,2007. <br /> The plant electrician visited the GTF on May 31,2007,and installed time-delay relays at both <br /> extraction wells. The purpose of the time-delay relays is to prevent the extraction pumps <br /> from"hammering" on and off because of rapid fluctuations in the GTF radio signals. If the <br /> pumps stop because of external interference with the GTF radio signals,the time-delay <br /> relays direct the pumps to remain off until they have observed a consistent radio signal for a <br /> specific period of time. The pumps will then restart. The time-delay relays were initially set <br /> for a delay period of one minute. <br /> Beginning in early June 2007,excessive noise was observed on the GTF autodialer phone <br /> line. AT&T performed troubleshooting on June 14,2007, and detected a problem with the <br /> phone line. AT&T successfully repaired the phone line on June 15,2007. <br /> During a site visit on June 15,2007,a very slow drip leak was observed at the influent <br /> header pipe,and both extraction wells were cycling on and off at approximately the same <br /> time.The leak was located adjacent to the air stripper,and came from a threaded,plugged <br /> connection to the former acid injection system.The GTF continued operating until it was <br /> shut off on June 16,2007.The threaded plug was replaced on June 16,but the slow drip leak <br /> continued.The section of header pipe where the leak occurred was then replaced on June <br /> 16.The GTF remained off to allow the pipe solvent cement to cure. The GTF was restarted <br /> on June 18,2007. <br /> During an inspection of the GTF on June 25,2007,a leak was discovered at the EW-2 <br /> wellhead pressure gauge, and EW-2 was turned off. The leak occurred through the handle <br /> of a ball valve located directly beneath the pressure gauge. Some water leaked onto the <br /> access road adjacent to EW-2,but none of the leaking water entered the stormwater ditch <br /> opposite EW-2 or Littlejohn Creek. The ball valve was replaced and EW-2 was restarted on <br /> June 26,2007. <br /> An acid washing of the air stripper packing material is scheduled for the week of <br /> July 9,2007. This routine maintenance procedure removes mineral deposits,thereby <br /> improving the efficiency of the treatment system. Additional troubleshooting and repairs of <br /> the GTF radio controls are scheduled for the week of July 23,2007,to eliminate the <br /> interference and intermittent extraction well cycling that have affected the treatment system. <br /> The additional troubleshooting and repairs will include the following steps: <br /> • Installing new receivers equipped with built-in signal strength meters at both extraction <br /> wells <br /> • Verifying radio signal strength at both extraction wells <br /> RDD/071990021(NLH3536.DOC) 3 <br />