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ARCHIVED REPORTS_XR0006873
EnvironmentalHealth
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2900 - Site Mitigation Program
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PR0537485
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ARCHIVED REPORTS_XR0006873
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Last modified
7/27/2020 5:50:19 PM
Creation date
7/27/2020 3:49:05 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0006873
RECORD_ID
PR0537485
PE
2957
FACILITY_ID
FA0021568
FACILITY_NAME
FORMER RAINWATER CAR WASH
STREET_NUMBER
420
Direction
W
STREET_NAME
YOSEMITE
STREET_TYPE
AVE
City
MANTECA
Zip
95336
APN
21931206
CURRENT_STATUS
01
SITE_LOCATION
420 W YOSEMITE AVE
P_LOCATION
04
P_DISTRICT
005
QC Status
Approved
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EHD - Public
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' 01 October 2004 <br /> • AGE-NC Project No 97-0333 <br /> ' Page 4 of 11 <br /> Laboratory analysis of extraction and treatment effluent grab water samples did not detect any <br /> constituents of concern Analytical results are summarized in Table 1, laboratory reports are in <br /> Appendix A <br /> iUtilizing a Blue-White Industries F-2000 flow meter,total flow(totalizer)was recorded between 26 <br /> December 2003 and 10 March 2004(Table 5) During this time,the extraction and treatment interim <br /> ground water remediation system was in operation for approximately 75 days Based on the total of <br /> approximately 280,576 gallons of water recorded during this time, AGE estimated that an average <br /> 3,741 gallons of water was discharged per day during this time <br /> 2 6 MASS-VOLUME REMOVAL CALCULATIONS <br /> Between 26 December and 10 March 2003,an estimated 13 56 pounds of MTBE was extracted from <br /> ground water (Table 5), since the system was initiated on 21 January 2002, a total mass of 233 90 <br /> pounds of MTBE has been removed The December 2003 to March 2004 mass-volume calculations <br /> of MTBE-impacted ground water extracted from the ground water extraction and treatment system <br /> are presented in Appendix B Plots of cumulative ground water pump and treat mass removal trends <br /> and influent ground water MTBE concentrations versus time are in Appendix C <br /> ' 3.0. GROUND WATER MONITORING AND SAMPLING <br /> Between 31 March and 02 April 2004, ground water monitoring and sampling were performed at 46 <br /> ground water monitoring wells (MW-1 through MW-13) Quarterly ground water monitoring <br /> procedures for the site were outlined in the AGE-prepared Work Plan Addendum, dated 03 April <br /> 2002, prepared by AGE and approved by San Joaquin County Environmental Health Department <br /> (SJCEHD) by letter dated 12 April 2002 As-built monitoring well construction details are <br /> summarized in Table 6 <br /> 3 1 WELL MONITORING AND PURGE PROCEDURES <br /> ' On 31 March 2004 the depth to ground water was measured at each momtonn well from the to <br /> p 1� g p <br /> of each well casing to the nearest 0 01-foot utilizing a Solinst water level meter The ground water <br /> ' elevation in each monitoring well was calculated by subtracting the measured depth to ground water <br /> from the surveyed casing elevation(Table 2) Ground water elevation and vertical gradient data for <br /> wells MW-11, MW-12 and MW-13 are depicted in cross section F-F' (Figure 3), ground water <br /> elevations were plotted in plan view for the informal First Zone, Second Zone, Third Zone and <br /> Advanced GeoEnvironmental,Inc <br /> i <br />
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