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w <br /> 3.2 Hydrocarbons <br /> On July 6, eight to ten gallons of water were purged from each monitoring well before <br /> samples were collected During purging, the pH, temperature, and conductivity of the <br /> extracted water were measured with a Corning meter to insure that water samples would be <br /> representative of unaltered groundwater (Appendix A) To prevent cross-contamination <br /> from MW-2 to the more distant wells, MW-2 was purged and sampled last The water <br /> purged from the wells was stored on site in a 55-gallon drum The vapor extraction and <br /> sparging wells were purged of only 2 to 5 gallons prior to sampling because of their slower <br /> recharge rates Strong sewer odors were noted in S W-1 and SW-2, and the water was gray <br /> in color, suggesting that water from a buried sewer line is tapped by these wells Strong <br /> gasoline odors were also noted in SW-1 and MW-2 <br /> Samples were collected from all ten wells in sterilized vials, labeled, placed in a cooled ice <br /> chest, and transported to Sequoia Analytical Laboratories for hydrocarbon analysis <br /> Laboratory data are summarized in Table 2 The full laboratory report is included in <br /> Appendix B <br /> None of the five gasoline oxygenates were detected in any of the wells, confirming the <br /> results obtained during the first quarter monitoring in April Concentrations of gasoline and <br /> BTEX were lower in all wells except SW-1, which showed an increase in TPH-g from <br /> 13,800 to 59,700 despite decreases in concentrations of all aromatic compounds (benzene, <br /> etc ) Concentrations of all analytes decreased significantly in MW-2, and for the first time, <br /> concentrations in MW-2 have declined below those in SW-I <br /> Figure 4 is a benzene isocontour map for the samples collected on July 6 Comparing this <br /> map to the map prepared by the Clearwater Group prior to ORC injection(see Upgradient's <br /> First Quarter Report) ,the plume is smaller and more elongate than it was in 1997 <br /> The third quarterly monitoring and sampling event will take place in late September <br /> 3.3 Dissolved Oxygen <br /> Dissolved oxygen concentrations were measured on June 10 and again on July 6 in <br /> conjunction with quarterly monitoring A portable dissolved oxygen sensor was used to <br /> measure the concentration in percent DO and in milligrams per liter (mg/1) at 2-gallon <br /> intervals during purging The dissolved oxygen data are shown in Appendix A, and final <br /> readings at the conclusion of purging are tabulated in Tables 3 and 4 and plotted against <br /> time in Figure 5 In contrast to previous months, concentrations did not decrease during <br /> purging, indicating that standing water in the wells was no more oxygenated than water <br /> from deeper in the formation <br /> Concentrations were slightly higher in seven of the ten wells on June 10 than they had been <br /> on May 8, and were significantly higher in four of the ten on July 6 Only one well (VW-1) <br /> 3 <br />