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SR0083330_SSNL
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2600 - Land Use Program
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SR0083330_SSNL
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Last modified
3/9/2021 10:08:24 AM
Creation date
3/9/2021 10:01:08 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2600 - Land Use Program
FileName_PostFix
SSNL
RECORD_ID
SR0083330
PE
2602
FACILITY_NAME
10124 S PRIEST RD
STREET_NUMBER
10124
Direction
S
STREET_NAME
PRIEST
STREET_TYPE
RD
City
FRENCH CAMP
Zip
95231
APN
19322067
ENTERED_DATE
2/25/2021 12:00:00 AM
SITE_LOCATION
10124 S PRIEST RD
P_LOCATION
99
P_DISTRICT
001
QC Status
Approved
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EHD - Public
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22 December 2020 AdvancedGeo <br /> Project No. 20-6228 An Employee-Owned Company <br /> Page 8 of 15 <br /> 6.1. NUMBER OF PERCOLATION TESTS PERFORMED <br /> One shallow percolation test was performed at the site. The appropriate percolation test <br /> procedure established by the EHD was followed for the test (Procedure #3). The <br /> percolation test hole was pre-soaked overnight for 24 hours followed by two (2) one-hour <br /> percolation testing periods. <br /> 6.2. CONSTRUCTION OF PERCOLATION TEST HOLE <br /> On 10 December 2020, one boring was advanced for a shallow percolation test. The <br /> boring was advanced using a four-inch diameter hand auger to a depth of 42 inches bsg. <br /> Following borehole advancement, the sides of the boring were scraped, and loose <br /> material was removed from the borehole. Once the borehole was cleared of loose <br /> material, two inches of fine gravel was added to the borehole. The borehole was then <br /> filled with water to a depth of 12 inches above the gravel at the time of 0830. The test <br /> hole was then covered for 24 hours to allow for complete saturation of the borehole. <br /> 6.3. DESCRIPTION OF THE PERCOLATION TEST HOLE - POST SOAK <br /> On 11 December 2020, the boring was found to be completely dry, intact and in good <br /> condition. <br /> 6.4. PERCOLATION TEST CONFORMED TO SJC POLICY EHD 98-02 <br /> The work was performed in accordance with San Joaquin County Division 11 <br /> Section 9-1105.2 (d) General Requirements. <br /> On 11 December 2020, the percolation test hole was dry after sitting overnight. <br /> Percolation test procedure#3 was performed by adding water to approximately six inches <br /> above the gravel and recording the amount of water remaining in the borehole after 10- <br /> minute intervals for one hour, then at 5-minute intervals for one hour. The water level was <br /> measured from a fixed reference point at the surface of the boring using a Solinst water <br /> level meter. The final measurement was observed by the EHD inspector. Based on the <br /> field measurements collected, the percolation rate for the parcel was calculated; the <br /> Percolation Test Rate Field Sheet is provided in Appendix C. <br /> 6.5. COMPLETED PERCOLATION TEST FORM <br /> After completion of the test, the EHD inspector reviewed the field data and signed the <br /> required EHD Percolation Test Rate form. Field measurements recorded during the test <br /> are included on the Percolation Test Rate Field Sheet provided in Appendix C. <br />
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