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Date <br />6/x,2/61 <br />6/13/61 <br />FORM 103 <br />SUBMIT IN DUPLICATE <br />STATE OF CALIFORNIA <br />DEPARTMENT OF NATURAL RESOURCES <br />DIVISION OF OIL AND GAS <br />History of Oil or Gas Well <br />BALM CCiRI-I )iiATI CST 'UES T 721LIA a s <br />OPERATOR------- - — ---- <br />----------------- ------------------------------------- FIELD -------- <br />Well No. <br />i , Y06 -NG 2-3 20-- <br />— -------------- Sec. - ---------- 3S LSE <br />- , �'• ----------- ---B. & M. <br />August 231, 61 <br />Date--- — — ---- — — — <br />110 BJ4G* pu1.1.8rta[3, Cal.i.fmmu LArxrt 6-1002 <br />--- �`eeid"lt <br />---------- <br />(Telephone Number) -----------------`-- <br />(President, Secretary or Agent) — <br />It is of the greatest importance to have a complete history of the well. Use this form to report a full account of all important operations during the <br />drilling and testing of the well or during re -drilling, altering of casing, plugging, or abandonment with the dates thereof. Be sure to include such items <br />as hole size, formation test details, amounts of cement used, top and bottom of plugs, perforation details, sidetracked junk, bailing testa, shooting and <br />initial production data. <br />a98%'. - !1288 P.B. - Co INt�r <br />14c.:1 gas c _ g r./cf) <br />II'SI OTULls 3900 211 eT al,ss 2565 psis. <br />IH oV419 2565, IST. equals 255, IF oq als 60, <br />FF equals 60, <br />"an guage ring prior to running w.Lre line Baker bridge P:Lugf mould not, below � <br />Ran bit sand sc raperr and scraped casing 4273' - 43270. 4 -ran g �� • <br />below 42831'. i4m mccullough magnesium bridge plug aryl let at 128$ ,rte; �°uld not ga <br />- IM71 F <br />�+ %o*AaW!t.&Wa -j.R�Wma 4 42721 and h2761 . t <br />s <br />70 tester and Bet Packer at -4081 with tail to '; used 630' mad cushion. Took <br />1,/2 hour initial shut -U* 1 p�sfsure. 1%20 B. <br />9:25 ASM , June 12, 61 f Mae ste��d31�dn; shing blow with gas to ii' bean f� 7, i�aur 25 i�ixtof�a at <br />about 10 Minutes( rate too s=111 to measure). Took 1/2hour fines sh ado in <br />Recovered 2740' rat riga (2571 drill.n fluid and + Prsamir. <br />I.�1 equals 222,, zsI egaals 1870 IF Q g �t83 salt water with soarer sagd). <br />equals ��5 psis. ,a 518,' e,7,s 1btX), �`sI ec�ualss 1755,, Fii <br />e ring to 4235'. Attermptadtoset Bahr wire "no bridee Plug at 4213 r <br />did not set; stuck at 3%72' on why Out of hole, a'1aLW 13ne out of socket. f over.. <br />d[blo'P d P� to 4273', set P1uc and retrieved collar locator and setting too,. <br />•yet ►"alliburton chart-irm body briLlge plug at 4X7'. <br />itoduetion Tests Shot 4-4,/2" j©t 110108/ft. 28451 - , Too 28501* i'�art castor with 950' waterc'aahi.an and set Packer at 2813' with tail to 2811.(? <br />) 3/2 lir :.nidal shut-d.n <br />Pressure. Opened ten ter on 1,/2" B.H. boan for 1/2 hour at 2 =310 A,2,.0 .0 June 13, 1961, <br />weak 1j,, i©ow' Recovered 126 <br />' (30f) not rise- drilling fluid. Iii equals <br />r ': IF equals 475, FF aqt au 475,, �1 2403 <br />o.k, fast o«k. Psi.g• charts <br />Laid darn tubing, Removed . Cut 7" and 31 <br />Plawd l0' cement , 4-a/2-11 cam' 3:' below Fouad le, <br />abandoned wail tTtu� 1,3� of I1..112 and 7" caarings, we3,ded an steel cap and <br />