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COMPLIANCE INFO_2022
EnvironmentalHealth
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2300 - Underground Storage Tank Program
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PR0231021
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COMPLIANCE INFO_2022
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Entry Properties
Last modified
12/28/2022 4:49:35 PM
Creation date
1/27/2022 8:11:19 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2300 - Underground Storage Tank Program
File Section
COMPLIANCE INFO
FileName_PostFix
2022
RECORD_ID
PR0231021
PE
2361
FACILITY_ID
FA0003625
FACILITY_NAME
ARCO STATION #83560*
STREET_NUMBER
2908
Direction
W
STREET_NAME
BENJAMIN HOLT
STREET_TYPE
DR
City
STOCKTON
Zip
95207
APN
09763032
CURRENT_STATUS
01
SITE_LOCATION
2908 W BENJAMIN HOLT DR
P_LOCATION
01
P_DISTRICT
002
QC Status
Approved
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SJGOV\gmartinez
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EHD - Public
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S A N J O A Q U I N Environmental Health Department <br /> C:0 u N I Y AMENDED <br /> 4/27/2022 <br /> Underground Storage Tank Program Inspection Report <br /> Facility Name: Facility Address: Date: <br /> ARCO STATION#83560* 2908 W BENJAMIN HOLT DR, STOCKTON January 26, 2022 <br /> SUMMARY OF VIOLATIONS <br /> (CLASS I,CLASS II,or MINOR-Notice to Comply) <br /> Item# Remarks <br /> 310 CCR 2636(f)(4) Failure to meet monitoring requirements in lieu of being tightness tested every 12 months. <br /> OBSERVATION: The 323 sensor located in the transition sump did not shut down the 91 turbine and did not meet <br /> the requirements for annual line tightness testing exemption. <br /> REGULATION GUIDANCE:All pressurized piping with secondary containment shall be pressure tested at least <br /> once every 12 months at a minimum release detection of 0.1 gallons per hour at 150 percent of the normal <br /> operating pressure. Continuous monitoring systems that are fail safe and shut down the pump when a leak is <br /> detected, or optionally stop the flow of product at the dispenser if the leak is in the under dispenser containment <br /> (UDC), shall satisfy the requirement for annual line tightness testing. <br /> CORRECTIVE ACTION: The service technician reprogrammed the monitoring panel to shut down the 91 turbine, <br /> which satisfies the annual line tightness testing requirement. Ensure that all leak detection equipment is properly <br /> programmed at all times. This was corrected on site. No further action required. <br /> This is a Class II violation. <br /> Overall Inspection Comments: <br /> An inspection report was provided to the facility operator on the day of inspection. The report was amended <br /> and replaces the initial report. #308 was removed and #310 was added. All violations have been resolved. No <br /> further action required. <br /> Documents provided during inspection: Return to Compliance certification, flyer for free CUPA classes, invoice <br /> AFTER THE COMPLIANCE DATE, EHD WILL BILL FOR ALL TIME AND ACTIVITIES ASSOCIATED WITH BRINGING <br /> THIS FACILITY BACK INTO COMPLIANCE. <br /> THIS FACILITY IS SUBJECT TO REINSPECTION AT ANY TIME AT EHD'S CURRENT HOURLY RATE. <br /> Received by: Date: April 27, 2022 Inspector: Inspector Phone: <br /> Printed Name and Title: LYDIA BAKER, REHS (209)616-3046 <br /> Emailed to Lawrence Wight, President <br /> FA0003625 PR0231021 SCO01 01/26/2022 <br /> EHD 23-01 Rev.12/06/2021 Page 5 of 5 Underground Storage Tank Program OIR <br /> 1868 E. Hazelton Avenue I Stockton, California 95205 1 T 209 468-3420 1 F 209 464-0138 1 www.sjgov.org/EHD <br />
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