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ARCHIVED REPORTS XR0012541
Environmental Health - Public
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EHD Program Facility Records by Street Name
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2900 - Site Mitigation Program
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PR0543844
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ARCHIVED REPORTS XR0012541
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Last modified
10/23/2018 2:14:21 PM
Creation date
10/23/2018 11:24:13 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS XR0012541
FileName_PostFix
XR0012541
RECORD_ID
PR0543844
PE
2959
FACILITY_ID
FA0006174
FACILITY_NAME
Best Express Foods Inc.
STREET_NUMBER
2651
Direction
S
STREET_NAME
AIRPORT
STREET_TYPE
WAY
City
STOCKTON
Zip
95206
APN
16912003
CURRENT_STATUS
02
SITE_LOCATION
2651 S AIRPORT WAY
P_LOCATION
01
P_DISTRICT
001
QC Status
Approved
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EHD - Public
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w <br /> W <br /> Y. <br /> I <br /> MWOM <br /> M <br /> 94 <br /> L+7 <br /> ^ Prior to sampling, tra well was developed ter' purging a tctal <br /> .. of cne well casing volu,.e. Development volumes were reduced <br /> ; . from the five used in Phase I, to one, when it became apparent. <br /> LA that neither well was capable of yielding signiti.icant amounts <br /> of water. Development ,rater was periodically mor:itored for PH <br /> and electrical conductivity, and drummed onsite for ultimate <br /> disposal pending analytical results. <br /> t � <br /> F' A ground water sample from each well was collected immediately <br /> after development. Upon col�?ction, groundwater samples were <br /> + stored on ice, and delivered that day to Anlab, Sacramento, <br /> ! + for chemical analyses. <br /> ; , 4 . 2 LITHOLOGIC SEQUENCE AND FIRST GROUNDWATER <br /> Boring logs for all threemonitor wells are presented in the <br /> �w+ <br /> Appendix. Briefly, the subsurface strata consist primarily of <br /> sandy clays and silty ;ands of variable moi.sture content <br /> through a depth of 95 feet . <br /> For M11-1 , both coarsest lithologic units and elevated '.INu <br /> readings, as shown in :Table 4-2 and Figure ..4--3, were <br /> i � associated primarily with the depth interval' <br /> 65-75 ft, and <br /> s,. served as the basis for setting the well screen interval at a <br /> depth sufficient to intersect this lithologic sequence. z <br /> should be noted however, that HNu instrument malfunction <br /> prevented PID readings over the entire boring (during Phase <br /> b. <br /> I ) . Similarly, field evaluation of moisture content did not <br /> suggest the need for a sha-1.1over screening interval, to the <br /> j onsite geologist. During Phase I1', field HNu readings were <br /> inconclusive, and were not used in determining screening <br /> interval. <br /> After well completion and development, water levelrnc overed <br /> ;,. <br /> to a depth of approximately 31 feet below ground surface 11111- <br /> �.: 1 '9a.i:fir level was subsequently remeasured on July 27, 6 P1'1, <br /> 4-7 <br />
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