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Pacific Gas and <br /> Electric Comp y <br /> 1 Technical and Ecdlogiial Seiv�ce5 �3a-malmItCanvon Road <br /> rj'�r_ <br /> rf 'San Ramon,CA 94583 <br /> 00 JUL 31 PM ..25123.2000 <br /> July 26,2000 f7 [ 3 <br /> Ms. Mary Serra <br /> California Regional Water Quality Control Board <br /> Central Valley Region <br /> 3443 Routier Road, Suite A <br /> Sacramento,CA 95827-3003 <br /> Re: Second Quarter 2000 Groundwater Monitoring Report <br /> Pacific Gas and Electric Company's <br /> McMullin Gas Dehydrator Station,Manteca, CA <br /> Dear Ms. Serra: <br /> Enclosed is the Second Quarter 2000 Groundwater Monitoring Report for Pacific Gas and Electric Company's <br /> McMullin Gas Dehydrator Station. In August 1998, a compound formulated by Regenesis®called Oxygen <br /> Releasing Compound (or ORC)was injected at this site to enhance biodegradation rates in the subsurface. <br /> The following is a summary of field and laboratory results performed in May 2000: <br /> • TPH-gas, TPH-diesel, and BTEX were not detected in the samples collected from well MW-1,MW-3, <br /> MW-4, and PZ-1. <br /> • Gasoline-range hydrocarbons were detected in the sample collected from well MW-2 at a'concentration <br /> of 2,200 micrograms per liter(gg/L). <br /> • Unknown gasoline-range hydrocarbons were detected in the samples collected from wells MW-5, <br /> MW-6,MW-7,and MW-8 at concentrations of 280 gg/L, 1,300 gg/L, 480 gg/L, and 54 gg/L(<50 <br /> gg/L dup.), respectively. <br /> • Early diesel-range hydrocarbons were detected in the samples collected from wells MW-2,MW-5,MW-6, <br /> and PZ-4 at concer_trations of 6,600 gg/L, 1,900 gg/L, 260 gg/L, and 340 gg/L, respectively. <br /> • Benzene was detected in the samples collected from wells MW-2, MW-5, MW-6, and MW-7 at <br /> concentrations of 16 gg/L, 3.2 gg/L, 6.9 gg/L,and 20 gg/L,respectively. <br /> Toluene was detected in the sample collected from well MW-2 at a concentration of 3.1 gg/L. <br /> • Ethylbenzene was detected in the samples collected from wells MW-2,MW-6, and MW-7 at <br /> concentrations of 89 gg/L, 22 gg/L,and 3.4 gg/L, respectively. <br /> • Total xylenes were detected in the samples collected from wells MW-2, MW-6, and MW-7 at <br /> concentrations of 160 gg/L, 34 gg/L, and 5.3 gg/L,respectively. <br /> • Lead was not detected in any of the groundwater samples. <br /> • The direction of groundwater flow was to the west-southwest, with a hydraulic gradient of approximately <br /> 0.001 foot per foot. <br /> 402 331-00 168.doc <br />