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' Atlantic Richfield Company 8 <br /> ARCO 4932,16 E Harding Way,Stockton,CA June 7 2002 <br /> mg/kg (EW-1, 27 5') Petroleum hydrocarbons-were not detected above - <br /> laboratory reporting limits in the deepest sample collected from the boring for <br /> well DMW-1 at 80 feet bgs <br /> • Fuel oxygenates were detected in soil samples collected between 15 feet and <br /> ' 69 5 feet bgs in the boring for well DMW-1, and in all samples collected from <br /> the boring for EW-1 MtBE was detected 1n soil samples collected between 30 <br /> feet and 69 5 feet bgs in the boring for well DMW-1, and in all samples <br /> rcollected from the boring for well EW-1, at concentrations ranging from 0 24 <br /> mg/kg (EW-1, 47 5') to 290 mg/kg (EW-1, 27 5') A concentration of TBA was <br /> detected 1n the 15-foot sample from DMW-1 at 4 1 mg/kg All other fuel <br /> oxygenates were not reported above laboratory detection limits <br /> • Concentrations of BTEX constituents were reported in groundwater samples <br /> collected from wells EW-1 and DMW-1 Elevated concentrations of BTEX <br /> constituents were detected 1n well EW-1 at 9,900 ug/i, 40,000 ug/l,4,700 ug/l, <br /> and 24,000 ug/l, respectively A minor concentration of benzene was reported <br /> in samples collected from DMW-1 at 9 6 ug/l Due to raised detection limits as <br /> a result of elevated detections of MtBE,TPHg and/or other BTEX constituents <br /> ' were not detected 1n the wells <br /> • MtBE was detected 1n groundwater samples collected from wells DMW-1 and <br /> '. EW-1 at concentrations of 230 ug/1 and 520,000, respectively A concentration <br /> of TBA was reported 1n well DMW-1 at 93 ug/1 All other fuel oxygenates were <br /> not detected above laboratory reporting limits <br /> ' • Approximately 6,300 gallons of purge water and groundwater generated during <br /> aquifer testing, and approximately 4 32 tons of soil were transported by Dillard <br /> ' to 1nStrat for disposal <br /> VARIANCES TO THE JANUARY 15, 2002 AND MARCH 11, 2002 WORK <br /> ' PLAN SUBMITTALS, AND FEBRUARY 14, 2002 SJCEHD LETTER—SITE <br /> ASSESSMENT <br /> • Well Construction. According to SECOR's January 15, 2002 work plan and <br /> subsequent SJCEHD letter dated February 14, 2002, the proposed extraction <br /> well (EW-1) and deep monitoring well (DMW-1) were to be )Installed and <br /> ' completed at approximately 50 feet and 77 feet bgs, with screen intervals of <br /> approximately 25 feet to 50 feet bgs and approximately 72 feet to 77 feet bgs, <br /> ' respectively However, based on soil stratigraphy beneath the site, wells were <br /> completed at depths of approximately 44 feet and 81 feet bgs, with screen <br /> intervals of approximately 21 feet to 44 feet bgs, and approximately 75 feet to <br /> ' 80 feet bgs, respectively <br /> I1ARCO149321ReportslAsmt&AgfrTstRpt doc <br />