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v <br /> ENVIRONMENTAL HEALTH DEPARTMENT <br /> SAN JOAQUIN COUNTY Unit Supervisors <br /> , 1 a,?i Donna K Heran,R E H 5 304 East Weber Avenue,Third Floor <br /> Carl Borgman,R E H S <br /> H' ADrrector Mike Huggins,R E H S,R D I <br /> • Al Olsen,R.E H s Stockton, California 95202-2708 Douglas W Wilson,R E H S <br /> e P` Program Manager Telephone (209) 468-3420 Margaret Lagono,R E H S <br /> 4�rFoa` Laurie A Cotulla,R E H S Fax (209) 464-0138 Robert McCiellon,R E H S <br /> Program Manager Mark Barcellos,R E H S <br /> PAUL SUPPLE NOV 0 7 2002 <br /> ATLANTIC RICHFIELD COMPANY <br /> PO BOX 6549 <br /> MORAGA CA 95470 <br /> RE ARCO Station 4932 SITE CODE 11136 <br /> 16 E Harding Way <br /> Stockton CA 95204 <br /> San Joaquin County Environmental Health Department (SJCIEHD) has reviewed the <br /> "Site Assessment and Aquifer Testing Results" dated June 7, 2002 and the "Problem <br /> Assessment Report" (PAR) dated August 29, 2002 that were prepared on your behalf by <br /> SECOR International Incorporated (SECOR) and has the following comments <br /> • The June 7, 2002 report documents the installation of one deeper screened monitoring <br /> well (DMW-1) and one groundwater extraction well (EW-1) in March 2002, and the <br /> performance of a step-drawdown and constant rate pumping test in April 2002 DMW-1 <br /> was installed to monitor for possible vertical migration of the onsite groundwater <br /> contamination documented to extent to at least 50 feet below surface grade in soil boring <br /> SBA, and to be present in onsite shallow groundwater monitoring wells MWA thru <br /> MW-4 EW-1 was installed to perform the aquifer testing <br /> Analytical results from the soil sample collected at 80 feet below surface grade (bsg) <br /> from boring DMW-1 confirmed the non-detect results at depth from deep soil borings SB- <br /> 1 and SB-2 that were advanced on-site in July 2001 Analytical results from the initial <br /> groundwater samples collected from DMW-1 were 9 6 parts per billion (ppb) benzene <br /> and 140 ppb methyl tertiary butyl ether (MtBE) <br /> The step-drawdown test was performed to determine the appropriate pumping rate to <br /> use for the constant-rate pumping test This rate was determined to be 6 gallons per <br /> minute, and the constant rate pumping test was initiated at this rate However, as the <br /> test progressed it became necessary to decrease the pumping rate to prevent <br /> dewatering of the well The rate was decreased to 5 5 gallons per minute, and then to <br /> 4 5 and finally 4 0 gallons per minute The remainder of the test was performed at this <br /> rate Based on the drawdown measured in the selected observation wells, SECOR <br /> calculated a capture zone radius of 31 feet and 48 feet in the down-gradient and cross- <br /> gradient directions, respectively With the installation of additional extraction points, <br /> SECOR recommends groundwater extraction as an effective remedial alternative for <br /> mitigation of the petroleum hydrocarbon impact at this site MCF&R-w <br /> MI <br /> Nov 1 1 2002 <br /> BY.-------------------. <br />