Laserfiche WebLink
Sacramento, California Initially, groundwater depths were measured in each <br /> well using an electronic well sounder and the potential presence of free-phase <br /> petroleum product was determined There was no free-phase petroleum <br /> product observed in any well <br /> Prior to sampling, at least 3 well volumes of groundwater were purged from <br /> each well using a clean, dedicated bailer Purge water was placed in 55-gallon <br /> drums, sealed and temporarily stored onsite for future disposal <br /> Groundwater samples were collected from each well using that dedicated <br /> bailer Samples were placed in clean glass containers, which were sealed, <br /> labeled and stored in an iced chest for chain-of-custody delivery to Acculabs <br /> for BTEX, TPHg and oxygenates analysis <br /> 10 <br /> March 2002 <br /> Subsurface Site Investigation <br /> 1717 South Center Street-Stockton,California <br /> Prepared by Philip Services Corp <br /> N 1ENV1624001321121382EG\PmjxtslstockCmt4narch2042mvauganon doe May 14 2002 <br />