My WebLink
|
Help
|
About
|
Sign Out
Home
Browse
Search
ARCHIVED REPORTS XR0001263
Environmental Health - Public
>
EHD Program Facility Records by Street Name
>
C
>
CHARTER
>
441
>
2900 - Site Mitigation Program
>
PR0544208
>
ARCHIVED REPORTS XR0001263
Metadata
Thumbnails
Annotations
Entry Properties
Last modified
3/1/2019 5:05:30 PM
Creation date
3/1/2019 4:11:51 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0001263
RECORD_ID
PR0544208
PE
2957
FACILITY_ID
FA0003628
FACILITY_NAME
ARCO STATION #2168*
STREET_NUMBER
441
Direction
W
STREET_NAME
CHARTER
STREET_TYPE
WAY
City
STOCKTON
Zip
95206
APN
14707607
CURRENT_STATUS
02
SITE_LOCATION
441 W CHARTER WAY
P_LOCATION
01
P_DISTRICT
001
QC Status
Approved
Scanner
WNg
Tags
EHD - Public
There are no annotations on this page.
Document management portal powered by Laserfiche WebLink 9 © 1998-2015
Laserfiche.
All rights reserved.
/
85
PDF
Print
Pages to print
Enter page numbers and/or page ranges separated by commas. For example, 1,3,5-12.
After downloading, print the document using a PDF reader (e.g. Adobe Reader).
View images
View plain text
lY <br /> Cumulative FP Recovered to Date NA <br /> Approximate Depth to Groundwater 22 77 to 26 82 <br /> Direction of Groundwater Flow Northeast to East <br /> Groundwater Gradient 0 001 to 0 003 <br /> SVE QUARTERLY OPERATION AND PERFORMANCE <br /> Equipment Inventory King, Buck&Associates MMC5A(100 scfm) <br /> Operating Mode Catalytic <br /> SJVUAPCD Permit No N-3664-1-0 <br /> TPHG Conc at End of Period (lab) 14,000 mg/m3 <br /> Benzene Conc End of Period (lab) 190 Mg/M3 <br /> Flow Rate End of Period 25 cubic feet per minute re-dilution <br /> Applied Vacuum This Period 19 inches of water <br /> HC Destroyed this Period (lab) 1,880 pounds <br /> Utility Usage <br /> (electrical/gas/propane) 6,177 kilowatt hours <br /> Operating Hours This Period 936 <br /> Percent Time Operational 61% <br /> Number of Auto Shutdowns 2 (1-power failure, 1-high tem <br /> CURRENT SOURCE (BEFORE DILUTION) INFLUENT SUMMARY(LAB) <br /> TPHG Conc This Period 27,666 66 mg/m3(average) <br /> TPHG Conc Last Period NA <br /> Initial TPHG Conc 55,000 mg/m3 (January 24, 1997 [following system <br /> startup)) <br /> Benzene Conc This Period 51333 Mg/M3(average) <br /> Benzene Conc Last Period Not applicable <br /> Initial Benzene Concentration 980 mglm3(January 24, 1997[following system startup]) <br /> DISCUSSION <br /> Results of this groundwater monitoring event indicate that levels of dissolved gasoline hydrocarbons are <br /> consistent with levels detected during previous sampling events The groundwater flow direction and <br /> gradient are consistent with previous sampling events Groundwater elevation increased approximately <br /> 4 0 feet from the previous sampling event (November 1996) <br /> The remediation system was started up on January 24, 1997 The remediation system consists of a <br /> King, Buck and Associates MMC5A Catalytic Oxidizer rated at 100-cubic-feet-per-minute The <br /> • remediation system is connected to vapor extraction wells VW-4 through VW-13 The system was <br /> operational for 61 percent of the time during the first quarter and extracted a total of 1,880 pounds of <br /> SAC1N 1PJO10805108051461 OBS-961cjb 1 Rev 0 6112197 <br />
The URL can be used to link to this page
Your browser does not support the video tag.