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during these activities. However,I was unable to identify any information in our historical files to confirm what this pipe <br /> is. We also checked the surroundings for any meter/pull boxes,but could not find any. <br /> Consequently, CRA is requesting a variance to destroy MW-5 by pressure grout instead of over-drilling methods as <br /> originally proposed. <br /> Thank you for considering this request. <br /> Larry <br /> From: Silva, Larry <br />,r Sent: Thursday, June 19, 2014 9:14 AM <br /> To: 'Gabriel Gonzalez [EH]' <br /> Cc: Adrienne;Ellsaesser [EH] <br /> Subject: RE: 620 West Charter Way, Stockton <br /> Gabriel, <br /> This morning when clearing well MW-5 for over-drill,we located a 4-inch diameter line adjacent to well casing(see <br /> attached picture). It is located approximately 1.5 fbg. At this time, I'm uncertain what this line is for. It's not connected <br /> to MW-5. It also wasn't picked up in our pre-field subsurface utility clearance activities. Based on how it's located <br /> adjacent to MW-5, it appears to have been installed after MW-5 was installed. <br /> I'm in the process of gathering more information. We will likely request a variance to destroy MW-5 by pressure grout <br /> methods. I will let you know what I find. <br /> Thank you, <br /> Thank you, <br /> Larry . <br /> From: Silva, Larry <br /> Sent: Wednesday, June 18, 2014 5:59'PM <br /> To: 'Gabriel Gonzalez [EH]' <br /> Subject: RE: 620 West Charter Way, Stockton <br /> Hi Gabriel, <br /> Due to the subsurface utilities that were identified adjacent to.wells IVIW-3 and MW-7, CRA requested a variance to <br /> destroy these wells by pressure grout versus over-drilling methods. Yesterday Wiscussed with you over-drilling these <br /> wells by installing a 5-foot section of casing and drilling through it. The casing would act as a guide so augers do not <br /> wander and potentially damage nearby utilities. <br /> However,after obtaining additional details this afternoon,I would like to revert to our previous request to not over-drill, <br /> but to pressure grout these wells for the following reasons: <br /> • Well MW-3 is only 13 inches away from the closest marked utility(electrical). The utility trench may only be 7 <br /> inches away. An AT&T line was also marked 2 feet away. Turns out well MW-3 was not installed in the center of <br /> well box, but was installed more to the west and is actually closer to marked utilities than thought. <br /> • Well MW-7 is located 26 inches away from electrical line.The utility trench may only be 20 inches away. <br /> • An distance of approximately 24 inches in diameter will be needed to install casing. Due to the close proximity of <br /> the utilities,there is a high likelihood of encountering pea gravel in the utility trenches,which will make <br /> installation of casing problematic. <br /> 2 <br />