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ARCHIVED REPORTS XR0004808
Environmental Health - Public
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MADISON
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2900 - Site Mitigation Program
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PR0521765
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ARCHIVED REPORTS XR0004808
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Last modified
5/6/2019 4:45:01 PM
Creation date
5/6/2019 4:33:53 PM
Metadata
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Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0004808
RECORD_ID
PR0521765
PE
2950
FACILITY_ID
FA0014781
FACILITY_NAME
CARANDO MACHINE WORKS
STREET_NUMBER
420
STREET_NAME
MADISON
STREET_TYPE
ST
City
STOCKTON
Zip
95202
CURRENT_STATUS
01
SITE_LOCATION
420 N MADISON ST
P_LOCATION
01
QC Status
Approved
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EHD - Public
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! <br /> TreadvvelOW10 <br /> due to the presence of Fremont Street, and because of the proposed excavation depth below the <br /> water table <br /> The proposed excavation should remove all of the identified vadose zone soil contamination, <br /> ' much of the saturated soil contamination, and enable removal of some contaminated <br /> groundwater The proposed excavation area is underlain by approximately 7 5 to 10-feet of sand <br /> ! fill, followed by a silts and clays down to at least 34 feet bgs Groundwater recharge was slow 1n <br /> the borings, and it is expected that groundwater will flow relatively slowly into the excavation <br /> Residual soil impacts identified deeper than 23 feet bgs should be addressed by backfilling with <br /> ORC Excavation below 23 feet bgs will not be attempted because ORC backfill will address <br /> ! residual groundwater contamination, and because the shored excavation will be engineered for a <br /> set depth <br /> 54 Excavation Volumes <br /> The proposed excavation will generate approximately 512 cubic yards or 820 tons of soil It is <br /> estimated that 1 to 2 excavation volumes of water (one volume is 14' x 43'x 4') will be removed <br /> after soil excavation, or approximately 18,000 to 36,000 gallons of water The soil will be <br /> stockpiled and characterized for offsite disposal Clean, shallow soil may be re-used on site <br /> Clean import material will be used as backfill as needed While backfilling procedures will be <br /> determined by the project geotechnical engineer, we anticipate that the bottom 4 to 5 feet of <br /> excavation will be backfilled with pea gravel backfill and ORC compound <br /> 60 REMEDIATION SCHEDULE <br /> We can begin the excavation as soon as this workplan is approved by the SJCEHD The <br /> ! excavation would take approximately one week to shore and another 3 to 4 days to excavate <br /> The excavation will likely remain open 3 to 7 days to complete the dewatering Backfilling, <br /> recompaction and shoring removal will take an additional 4 to 7 days <br /> !R <br /> 9 <br /> 25971013 DGD 12 April 2004 <br />
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