Laserfiche WebLink
TABLET <br /> ESTIMATED VAPOR EXTRACTION SYSTEM HYDROCARBON MASS REMOVAL <br /> Valley Pacific Petroleum Services <br /> 930 Victor Road <br /> Lodi,California <br /> Page 2 of 2 <br /> Avg.Vapor Cumuleme Mau <br /> Dote Comment !lour Meter Period Hours CumWalive Avg.Flow 1n0uent PlD Influent Lab Period Mass Cotllment <br /> Hours (trial (PP-) a9fL) W��� Rermvetl(lbs) R(lbs)d <br /> 9/3/2013 O&M 5341.3 457.3 4,565.2 96 402 __ 362.2 6,724 Running OK <br /> 9/12/2013 O&M 5555.7 2144 4)]9.6 96 406 - 169.8 6,894 Rurming OK <br /> 920/2013 O&M 5]46.3 190.6 4,970.2 95 381 149.9 ],043 Running OK <br /> 9/2]201] Semple 5913.8 167.5 5,137.7 98 459 I,BW INUII 110.8 ],154 Running OK;sampled <br /> 10/11/2013 O&M 6251.1 337.3 5,475.0 95 430 216.3 7,3]0 Running OK <br /> 10/212013 O&M 6493.4 242.3 5,71].3 94 2501 153.7 7,524 Running OK <br /> 10282013 Sample 6658.8 165.4 5,882.7 94 402 1,300 1.3011 75.8 7,600 Running OK;sampled <br /> 11/7/2013 O&M 6900.0 241.2 6,1219 93 401 - 109.4 7,709 Running OK <br /> 11/182013 O&M _ _ - - - System was down m arrival. Could not restart. Rob Larson needs to troublesboot. <br /> 1120/2013 Re-Stan _ - - - Rob Urson found 2 of3 element banks burned out;wired up the third end re-stoned <br /> 11/25/2013 Searle 7214.9 314.9 6,438.8 1 100 311 660 660 77.9 7,787 Running OK;sampled <br /> 12/5/2013 O&M 7454.1 2]9.2 6,678.0 98 226 58.0 7,845 Running OK <br /> 1220/2013 Sample 7814.7 360.6 7,038.6 100 366 810 810 109.5 7,955 Running OK <br /> IN30/2013 O&M 8057.1 242.4 7,281.0 102 307 75.1 8,030 System Running OK;transfer pump does not work <br /> 1/32014 O&M 8147.7 90.6 7,371.6 100 - - 27.5 8,057 Down on arrival;would not heat up m restart attempt <br /> 12/12/2014 Re-Sun 8148.5 0.8 7,372.4 99 - - Maio installed new heating element and re-stinted unit,operating m all wells <br /> 12/30/2014 Sample 8580.7 432.2 7,804.6 99 105 290 290 46.5 8,104 System conning OK <br /> 1/29/2015 Sample 9293.4 712.7 8,517.3 99 88 210 210 55.6 8,159 1 System running OK,than recorder needs replacement <br /> 3/172015 Sample 10422.3 1128.9 9,646.2 98 115 270 270 112.0 8,271 System ruining OK,no power to char recorder <br /> 4/202015 Sample 11239.7 817.4 10,463.6 87 LIMO 5dato 5,000 1333.4 9,605 System running on VFW-ID since 4/10 <br /> 51182015 Sample 11912.1 672.4 11,136.0 87 397 3,600 3,600 789.7 10,394 System running on VFW-1D <br /> 6/152015 Semple 12583.6 671.5 11,507.5 83 802 4,600 4,600 961.4 11,356 Systemrunning on WW11) <br /> ]/9/2015 Sample 13156.0 572A 12,379.9 81 2,605 3,800 3800 660.7 12,017 System running on WW-ID <br /> 81132015 Sample tlY96J 840.1 17,220.2 ]6.5 951 3,600 1,600 867.8 12,884 System conning on VEW-ID <br /> 9/1U/2015 Sample 14671.1 674.8 13,895.0 76.1 700 3,900 7,900 751.0 13,635 System running on VEW-ID <br /> 10/82015 Sample 15341.1 670.0 14,565.0 72.7 690 3,300 3,300 602.8 14,238 System running on WW-ID <br /> 11/122015 Sample 16181.6 840.5 15,4055 86.2 48] 2,800 2,800 760.7 14,99Y Sysmm mooing on WW-ID <br /> 12/30/2015 Sample 1]337.0 1155.4 16,560.9 %5 488 2,1110 2,100 ]73.4 15,772 System running on WW-10 <br /> Notes: <br /> cfin =Cubic feet per minute <br /> Plus, =Pans per million <br /> ug/ =Micrograms per liter <br /> lbs -Pounds <br /> O&M =Operation&Maintenance <br /> • =Precut temp dropped below 600 on 6/22;post cut dropped below 600 on 6/27 <br />