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rate exceed the rate of water entry into the well This indicated that recharge to the well <br /> was less than 14 gpm and the 24 hour constant rate test would need to be less than 14 <br /> gpm The 24 hour constant pump rate was set at 0 725 gpm During the constant pump <br /> test it was noted that both the A and B zones were effected, indicating that the clay <br /> separating the two zones is a leaky aqurtard Using Cooper and Jacobs straight line <br /> method the transmxssivity (T) for the A zone calculated to be 28 fl/ day The A zone is <br /> approximately 5 5 feet thick which would calculate hydraulic conductivity (K) at 5 1 ft / <br /> day Using the gradient information obtained prior to any pumping MW2 to MW6A on <br /> January 21, 2003 ("7 79 ft--7 87 ft/91 ft = 0 00087 ft/ft) and an effective porosity of 20% <br /> (silt/fine sand) calculates a groundwater velocity (v) of 022 ft/day or 8 03 ft/year <br /> ZONE B <br /> The Step Drawdown tests were performed on the two separate water bearing zones to <br /> determine at what rate to conduct the 24 hours Constant Pump Rate tests Well RW1B is <br /> screened across the B zone and the step drawdown test was initiated at a pump rate of 0 8 <br /> gallons per minute (gpm) and was increased in 0 5 increments At 5 0 gpm field data <br /> indicated that enough information was available to determine the pump rate for the 24 <br /> hours constant rate test The 24 hour constant pump rate was set at 4 11 gpm During the <br /> constant pump test it was noted that both the A and B zones were effected Drawdowns <br /> where first seen in piezometer PZ1B and then in piezometer PZ2B and piezometer PZIA <br /> and then at RW 1A After which vertical leakage became the dominant observation <br /> r� Again indicating that the clay separating the two zones is a leaky aqumtard Using Cooper <br /> and Jacobs straight line method the transmmssmvmty (T) for the B zone calculated to be <br /> 1317 ft2 / day The B zone is approximately 8 feet thick which would calculate <br /> hydraulic conductivity (K) at 16 4 ft/day Using the gradient information obtained prior <br /> to any pumping MW2 to MW613 on January 21, 2003 (-7 79 ft--7 88 ft/92 ft = 0 00097 <br /> ft/ft and an o <br /> } effective porosity of 30/o (fine - medium clean sand) calculates a <br /> groundwater velocity(v) of 0 055 ft/day or19 95 ft/year <br /> AQUA TARD BETWEENA AND B ZONE SANDS <br /> As discussed above, the 3-4 foot thick aquatard separating the A and B zone sands is <br /> considered a leaky aquitard Core investigations of this zone showed the clay to have <br /> abundant silty content and at piezometer PZ213 to also have very fine sand associated <br /> with it The constant drawdown test on RW1B suggests that this zone impends flows in <br /> some areas and in other areas does not form a significant barrier for vertical leakage <br /> RESULTS OF OVER-EXCAVATION OF GASOLINE CONTAMINATED SOILS <br /> As shown on Figures 4A, 4B and 4C the excavation of gasoline contaminated soils <br /> occurred in stages Using a 15 foot reach backhoe, the first stage of excavating occurred, <br /> removing relatively clean over-burden to the 10 foot depth Gasoline impacted soils in <br /> the upper 10 feet were associated with the southern most pump island and the former <br /> UST area Once the area was excavated to the 10 foot depth a ramp was constructed at <br /> the eastern edge of the excavation area to access areas that would need to be excavated <br /> deeper The area containing piezometers PZ2A and PZ213 was then excavated to the 14 <br /> 9 Update Status March 2003 <br />