My WebLink
|
Help
|
About
|
Sign Out
Home
Browse
Search
SITE INFORMATION AND CORRESPONDENCE FILE 1
Environmental Health - Public
>
EHD Program Facility Records by Street Name
>
C
>
COUNTRY CLUB
>
2103
>
3500 - Local Oversight Program
>
PR0544591
>
SITE INFORMATION AND CORRESPONDENCE FILE 1
Metadata
Thumbnails
Annotations
Entry Properties
Last modified
6/21/2019 2:38:17 PM
Creation date
6/21/2019 11:32:02 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
SITE INFORMATION AND CORRESPONDENCE
FileName_PostFix
FILE 1
RECORD_ID
PR0544591
PE
3526
FACILITY_ID
FA0005220
FACILITY_NAME
CHEVRON #9-4054
STREET_NUMBER
2103
STREET_NAME
COUNTRY CLUB
STREET_TYPE
BLVD
City
STOCKTON
Zip
95204
APN
12308029
CURRENT_STATUS
02
SITE_LOCATION
2103 COUNTRY CLUB BLVD
P_LOCATION
99
P_DISTRICT
001
QC Status
Approved
Scanner
SJGOV\wng
Tags
EHD - Public
Jump to thumbnail
< previous set
next set >
There are no annotations on this page.
Document management portal powered by Laserfiche WebLink 9 © 1998-2015
Laserfiche.
All rights reserved.
/
249
PDF
Print
Pages to print
Enter page numbers and/or page ranges separated by commas. For example, 1,3,5-12.
After downloading, print the document using a PDF reader (e.g. Adobe Reader).
View images
View plain text
[eevmn <br /> Chevron <br /> Chevron U.SA Products Company <br /> 6001 Bollinger Canyon Rd., Bldg. L <br /> P.O. Box 5004 <br /> San Ramon, CA 94583-0804 <br /> She Assessment& Remediation Group <br /> July 12, 1995 Phone (510) 842-9500 <br /> Mr. Michael Infuma <br /> San Joaquin County Environmental Health <br /> P.O. Box 2009 <br /> Stockton, CA 95201 <br /> Re: Former Chevron Station#9-4054- 2103 Country Club Blvd Stockton CA <br /> Attached groundwater monitoring report(Blaine Tech, 3/27/95) <br /> Dear Mr. Infuma: <br /> Attached you will find a report dated March 27, 1995, which was prepared by Chevron's <br /> consultant, Blaine Tech Services, Inc. (Blaine Tech), to describe groundwater monitoring <br /> performed at the subject site on February 23, 1995. <br /> During their February site visit Blaine Tech gauged and sampled all seven site-related wells. The <br /> measured direction of groundwater flow was toward the northeast with a hydraulic gradient of <br /> 0.008 ft/ft. Each groundwater sample was analyzed for the presence of TPHGas and BTEX <br /> constituents. Detectable concentrations of dissolved hydrocarbons were measured at all seven <br /> wells. The measured concentrations were consistent with those measured during previous site <br /> monitoring events. The concentrations measured at MW-7 were greater than those detected during <br /> the fourth quarter, 1994 sampling event. The dissolved hydrocarbon concentrations at MW-7 <br /> during February were consistent with all other previous measurements. The lower than usual <br /> detections at this well during the previous quarter appear to be anomalous. No explanation for this <br /> anomaly is offered at this time. <br /> If you have any questions or comments,I can be reached at(510) 842-8695. <br /> Sincerely, <br /> d e- A0Zt- <br /> Brett L. Hunter <br /> Environmental Engineer <br /> Site Assessment and Remediation <br />
The URL can be used to link to this page
Your browser does not support the video tag.