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ARCHIVED REPORTS THIRD QUARTER GROUNDWATER MONITORING REPORT AUGUST 2015
Environmental Health - Public
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ARCHIVED REPORTS THIRD QUARTER GROUNDWATER MONITORING REPORT AUGUST 2015
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Last modified
6/25/2019 8:51:00 AM
Creation date
6/25/2019 8:25:41 AM
Metadata
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EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
THIRD QUARTER GROUNDWATER MONITORING REPORT AUGUST 2015
RECORD_ID
PR0009276
PE
2960
FACILITY_ID
FA0012033
FACILITY_NAME
PILKINGTON NORTH AMERICA
STREET_NUMBER
500
Direction
E
STREET_NAME
LOUISE
STREET_TYPE
AVE
City
LATHROP
Zip
95330
APN
19812008
CURRENT_STATUS
01
SITE_LOCATION
500 E LOUISE AVE
P_LOCATION
07
P_DISTRICT
003
QC Status
Approved
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EHD - Public
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' Table B-Historic Diesel Thickness Measurements and Product Recovery Data(06/18/99 through 9/30/15) <br /> Depth to Cumulve <br /> Date 'Recovery Depth <br /> Depth to Diesel DieselatiOperations and Maintenance Notes <br /> Well Diesel Grnundwarer Thickness Removed <br /> ' (gallons) <br /> RW-1 12.76 12.88 0.12 0.17 <br /> RW-2 Dry 50.47 <br /> 223/2015 RW-3 13.64 71.29 RW-2 was dry and RW-6 well casing damaged.Initial drum volume was approximately <br /> ' RW4 12.81 14.04 1.23 122.70 6.5 gallons of product.Ending drum volume was approximately 7.0 gallons of product. <br /> RW-5 12.74 <br /> RW-6 4.27 <br /> RW-1 12.47 12.51 0.04 0.17 <br /> RW-2 13.56 50.52 <br /> RW-3 13.55 7149 RW-5 buried under and;attempts to locate with mem l detector were unsuccessful RW-6 <br /> 3/4/2015 RW4 12.85 13.80 0.95 12320 well casing damaged.Initial drum volume was approximately 7.0 gallons of product. <br /> RW-5 Buried Ending drum volume was approximately 7.8 gallons of product. <br /> RW-6 Dry 1 4.27 <br /> ' 3/5/2015 RW-5 RW-5 located;appears to have been damaged with construction equipment.Temporary <br /> repairs made.RW-5 covered with a traffic cone and 0agging. <br /> RW-1 12.73 12.74 0.01 0.17 <br /> RW-2 13.58 13.80` 022• 50.52 <br /> 3/242015 RW-3 13.52 71.49 RW-6 dry and well casing damaged.Product drum not in shed;an product removed <br /> ' RW-4 12.85 13.82 0.97 123.20 during event.Initial and ending drum volume was approximately 7.8 gallons of product. <br /> RW-5 12.31 <br /> RW-6 Dry 4.27 <br /> RW-1 12.80 12.82 0.02 0.17 <br /> ' RW-2 13.60 14.30 0.70 50.64 <br /> RW-3 13.53 71.52 [)man was changed out RW-6 dry and well casing damaged.Initial drum volume was <br /> 3/312015 RW-4 12.85 13.90 1.05 123.58 approximately 0.0 gallons of product.Ending drum volume was approximately 0.5 <br /> RW-5 12.33 gallons of product. <br /> RW-6 Dry 4.27 <br /> RW-I 11.20 11.30 0.10 0.19 <br /> RW-2 Dry 50.67 <br /> 4/10/2015 RW-3 13.60 13.97 0.37 71.68 Product was recovered from RW-2 from the SoakEase sock that was installed to the <br /> RW-0 12.83 13.74 0.91 123.92 well. <br /> RW-5 13.36 <br /> ' RW-6 Dry 4.27 <br /> RW-1 12.85 12.86 0.01 0.19 <br /> RW-2 13.60 13.61 0.01 50.67 <br /> RW-3 13.43 13.65 0.22 71.99 <br /> 41172015 RW-4 12.89 13.50 0.61 124.08 No product was recoveredfrom RW-2.SoakEase sock N RW-2 recovered no product. <br /> ' RW-5 13.42 <br /> RW-6 Dry 4.27 <br /> RW-1 12.91 12.92 0.01 0.19 <br /> RW-2 13.60 13.65 0.05 50.69 <br /> ' <br /> 4/2312015 RW-3 13.43 13.57 0.14 72.01 <br /> RW-5 has been damaged.Top of well has been destroyed.Needs new well cap. <br /> RW4 12.90 13.51 0.61 124.28 <br /> RW-5 13.41 <br /> RW-6 D 4.27 <br /> RW-I 12.07 0.19 <br /> ' RW-2 13.61 50.70 <br /> RW-3 13.45 13.75 0.30 72.10 <br /> 4/28/2015 RW-1 was observed to be slightly pressurized. <br /> RW-4 12.89 13.58 0.69 124.49 <br /> RW-5 13.35 <br /> RW-6 Dry 4.27 <br /> ' RW-1 12.84 12.89 0.05 0.20 <br /> RW-2 13.70 14.15 0.45 50.72 <br /> RW-3 13.37 14.02 0.65 72.23 <br /> 5/5/2015 RWJ 12.95 13.53 0.58 124.68 RW-2 has obstruction inside well and cannot retrieve product with bailer. <br /> RW-5 13.42 <br /> ' <br /> RW-6 Dry 4.27 <br /> RW-1 13.02 13.07 0.05 0.20 <br /> RW-2 13.78 14.05 0.27 50.73 <br /> RW-3 13.74 14.20 0.46 72.43 <br /> 5/122015 RW4 13.04 13.56 0.52 124.82 Detected no water in RW 2.Product filled the well from the bottom. <br /> RW-5 13.49 <br /> RW-6 4.27 <br /> RW-I 13.11 13.16 0.05 0.20 <br /> RW-213.89 Dry 50.75 <br /> 5/2D2015 <br /> ' RW-3 13.79 14.34 0.55 72.60 <br /> SoakEase sock in RW-2 was damaged;replaced with new sack. <br /> RW-0 13.15 13.76 0.61 125.07 <br /> RW-5 13.52 <br /> RW-6 D 4.27 <br /> ' lkondecwmry public\Prolech7000y9O0e4 Janes Dev Co(previously PNA)\7064B Diesel RecovarykRopoft\3015\Table B.xls Page 32 of 34 <br />
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