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FIELD DOCUMENTS
Environmental Health - Public
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EIGHT MILE
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11540
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2900 - Site Mitigation Program
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PR0506051
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Last modified
7/10/2019 12:26:05 PM
Creation date
7/10/2019 10:29:10 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
FIELD DOCUMENTS
RECORD_ID
PR0506051
PE
2950
FACILITY_ID
FA0007171
FACILITY_NAME
HOLIDAY HARBOR/INTREPID MARINE
STREET_NUMBER
11540
Direction
W
STREET_NAME
EIGHT MILE
STREET_TYPE
RD
City
STOCKTON
Zip
95219
APN
07119004
CURRENT_STATUS
02
SITE_LOCATION
11540 W EIGHT MILE RD
P_LOCATION
99
QC Status
Approved
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EHD - Public
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lP <br /> 1 <br /> i� <br /> the levee under the deck .:ind stairs,along a retaining wall and waspuddling on the grass and into the roadway <br /> ' behind the levee." After considerable hand work under the deck,Falcon reported that"the diesel line was joined <br /> at a deep depth[below ground surface]at a juncture point by a rubber hose which had collapsed under the weight <br /> of the fill at that depth" The Falcon report recommended that the broken diesel line as well as two gasoline lines <br /> ' which also ran under the building should be capped. A representative from San Joaquin County Health Services <br /> Environmental Health Division (SJCEHD) inspected the purging andi capping of the fuel lines prior to the lines <br /> being capped. The fuel lines were then to be run aboveground. <br /> ' According to the 1991 Problem Assessment Report prepared by RESNA,a preliminary soils investigation of the <br /> King Island portion of the site consisted of hand augering 19 shallow soil borings around the marina and store <br /> buildings, the USTs and levee. Analytical results were not available for review but a later RESNA report <br /> indicated that free product was discovered in soil boring 10(SB 10)which was located between the Marina office <br /> and store buildings_ s <br /> ' A Tank Removal Report prepared by RESNA documented the removal of a 2,000-gallon,steel,Ieaded gasoline <br /> UST and associated piping from the King Island property in 1991. The report stated that the UST and piping <br /> was in good condition. Analytical results for the soil samples indicated non-detectable levels of TPH,,with.the <br /> ' exception of 0.045 mg/kg of toluene. Total lead was detected at concentrations up to 47 mg/kg. A hand written <br /> note attached to the February 20, 1992,UST unauthorized release report refers to a March 26, 1992 conversation <br /> with Tina LaPage of RESNA (currently Smith) in which it was discussed that lead concentrations would be <br /> ' ignored by the County since a closure report would not be issued based on the pipes remaining under-the building. <br /> It was noted that only if a way were found to test under the store could a closure report ever be issued on the <br /> removal. ` <br /> II <br /> RESNA installed Eve monitoring wells (MW 1-MWS)on the King Island property between March and April <br /> 1991 to determine whether groundwater had been impacted and if so to what extent. An additional monitoring <br /> ' well(MW6)was installed in September 1993 to further define groundwater contamination at the site.MW4 was <br /> abandoned and replaced in August 1995 due to an infiltration of organic debris. <br /> Review of Quarterly Monitoring Reports prepared between 1991 and 1994 indicated the following trends in <br /> analytical results. Samples collected from MW-I and MW-2 were.below detection limits for every sampling <br /> event. MW-3 has shown non-detectable concentrations for TPH and BTEX for every sampling event,with the <br /> exception of toluene and xylenes (0.9 and 2.4 µgip respectively) in the first sampling event. <br /> Concentrations up to 6,900 µg/k TPHg , 2,600 TPHd,and 3,300 benzene were detected in MW-4 from May <br /> ' 1991 through September 1993. Non-detectable concentrations for all analytes were seen in MW4 during the <br /> December 1993 sampling event. Concentrations of TPHg ranged from 160 to 260 µg/1 until the well was <br /> abandoned in 1995.The replacement well MW4R showed non-detectable concentrations for all analytes during <br /> the August 1995 sampling event. 'F <br /> Concentrations from 90 to 26,000µg/2 of TPHg,510 to 570 µg/2 TPHd,and 6.6 to 1,700 µg/2 of benzene were <br /> detected in MW5 from April 1993 through December 1993. MW5 showed non-detectable concentrations of TPH <br /> and BTEX during the June and December 1994 and the September`and October 1995 sampling events. <br /> ;j <br /> h:\wcaec5kikhlitiHtii.rp <br /> ' <br /> 50I33-001A2 <br /> #i <br />
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