Laserfiche WebLink
System Monitoring (January 1994 - March 1995) <br /> 141 N El Dorado Avenue <br /> Sal Vent System with Granulated Activated Carbon <br /> Air Permit to Operate No N-1132-2-0 <br />. Authority to Construct No N-1133-2-1 <br /> Air Permit to Operate Conditions Max Airflowrate 200 CFM, Max TPH cont = 32 ppmv (gasoline) or 168 ppmv (methane) <br /> Date rime Wells Fresh Soil Vapor Temp Pitot Tube Airflow Airflow Concentrauon Benzene TPH TPH TPH Cimiul TPH <br /> Open to Air Valves Extraction Velocity (avg) (avg # Influent Influeni Effluent Extraction Extraction Extraction <br /> Venting Condition Vacuum Pressure (4 in pipet (ppmv) (ppmv) (ppmO (pprnv) (lbsiday) (lbslday) Estimate Commems <br /> lin 1420 (de F! tin 1420 (ACFM) (SCFMv R civ ) tLAa) (LA 6) (Flo) (FIO) (LAR! fibs-LAS) <br /> 117194 9 30 1 VEW-1,2,3,4 closed 45 82 0 11 117 114 140 99 0 038 3 6 1167 <br /> 1127194 VEW-1,2,3,4 closed System shut down {1/27/941 <br /> 3117194 13 45 VEW-1,2,3,4 closed -40 75 0 16 141 140 207 110 ND(<0 16) 0 93 4 9 11674 Restarted system (3/17/94) <br /> after GAC replacement. <br /> 415194 11 15 VFW-1,2,4 closed -40 103 0 15 140 132 91 85 ND(<0 16) 0 39 36 1247 <br /> 4119/94 15 30 VEW-1,2,3,4 closed -40 109 0 16 145 135 160 98 6 9 <br /> S1319411 SO VEIN-1,2,3,4 closed -45 104 0 14 135 127 30 68 0 19 1 1 2 28 1337 <br /> 5117194 13 45 VEIN-1,2,3,4 closed -43 101 0 15 139 127 80 57 NO(<0 08) 58 33 2.3 1373 <br /> 611194 11 00 VEW-1,2,3,4 closed -43 117 0 14 137 126 44 51 0 41 1 2 is 21 1406 <br /> 6/13/948 30 VEIN-1,2,3,4 closed -43 117 0 14 137 126 40 1 1 6 System Shutcown <br /> 6113 - 718194 (6113 -7/8 94) for remediation <br /> system modifi4ation <br /> 7/111949 45 VEW-1,2,3,4,MW-3 partially open -31 74 0 6 153 152 56 24 NO(<0 16) 7 21, 1 2 14061 <br /> 8123194 15 30 VEW-1,2,3,4,MW-3 partially open 15 83 0 24 97 95 40 45 ND(<0 016) 0 1 2 1 4 1462 <br /> • 9120194 10 55 VEW-1,2 3 4 MW-3 closed 35 114 0 i6 146 135 38 45 ND(<0 016) 0 1 6 1 9 1508 <br /> 1014194 15 40 VEW-1,2,3,4,MW-3 closed 38 106 0 16 14S 136 26 34 ND(<0 016) 0 1 1 1 5 1532 <br /> 11/18/94 13 30 VEW-1,2,3,4 MW-3 closed 38 119 0 15 142 130 11 9 4 NO(<O 016) 0 0 5 0 4 1573 <br /> 11129 - 12116/94 1 System shut down due to <br /> 12/30/94 12.30 VEW-1,2,3,4 MW-3 closed -35 119 0 15 142 130 37 ND140 0801 1 S 1580 electncal problem on control <br /> 1130195 15 25 VEW-1,2,3,4,MW-3 closed 39 107 0 14 135 126 20 12 NDS<0 016) 0 08 05 1603 panel (11/29 -12/16/94) <br /> 217/95 14 15 VEW-1,2,3,4,MW-3 closed -43 106 0 14 135 126 11 16 ND(<0 016) 0 0 4 09 1607 <br /> 2123195 1616 Shut down system <br /> 319196 8 55 VEW-1,2,3,4,MW-3 closed 38 112 0 15 141 131 18 12 +1 038 0 08 0 5 1616 Restarted system <br /> Notes <br /> System consists of one regenerative blower with 5 hp motor and two 2000 Ib GAC units in series (Unit 1 and Unit 2) <br /> System start-up was conducted by Aegis Environmental (now Fugro West, Inc ) on 6/23/93 System was previously operated by Resna Industries <br /> avg. = average of three sets of measurements collected at 15 minute intervals <br /> GAC = granular activated carbon <br /> Airflow measured between Carbon Unit 1 and Unit 2 except on 7111/94 and 8/23/94 Airflow measured at the vent well manifold an 7111/94 and 8/23/94 <br /> Influent = prior to Unit 1/sod vent blower discharge <br /> Effluent = Unit 2 (atmospheric discharge) <br /> TPH = total petroleum hydrocarbons as gasoline <br /> ppmv = parts per million by volume <br /> FID-field measurement from flame ionization detector calibrated to hexane(Model- Century OVA 128 by Foxboro Company) <br /> LAB = laboratory analysts <br /> ND = not detected at indicated reporting limit <br /> " ACFM = actual cubic feet per minute " <br /> SCFM = standard cubic feet per minute (14 7 PSI and 70 deg F) <br /> PSI = pouncWsquare inch <br /> See attached extraction rate calculation <br /> Cumulative extraction is calculated by averaging extraction rates for consecutive sampling events and summing up previous total <br /> *Cumulative TPH extraction calculations do not include TPH extraction between 1/7-1/27 & 718-7/11/94 f <br /> For cumulative TPH extraction calculation after 12/30/94, system operation hours are esttmated based on field observations <br /> s <br /> i <br />