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3500 - Local Oversight Program
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PR0544683
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SITE INFORMATION AND CORRESPONDENCE
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Last modified
10/22/2019 3:12:46 PM
Creation date
7/22/2019 8:09:05 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
SITE INFORMATION AND CORRESPONDENCE
RECORD_ID
PR0544683
PE
3528
FACILITY_ID
FA0004953
FACILITY_NAME
NORMAC INC
STREET_NUMBER
6215
STREET_NAME
TAM O SHANTER
STREET_TYPE
DR
City
STOCKTON
Zip
95209
APN
09405011
CURRENT_STATUS
02
SITE_LOCATION
6215 TAM O SHANTER DR
P_LOCATION
01
P_DISTRICT
002
QC Status
Approved
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EHD - Public
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i <br /> I <br /> Case Closure Suxrnanaxy ^��(L � � '{ L 4 �� � <br /> Leaking Underground Fuel Storage Tank PrograM <br /> 1 Agency Information Date: <br /> Agency name:SAN JOAQUIN COUNTY PHS/EHD Address: 304 S WEBER AVE <br /> City/State/Zip: STOCKTON CA 95202 Phone: (209) 468-3442 <br /> Responsible staff person: H KNOLL Title: SENIOR RENS <br /> II. Case Information <br /> Site facility name: NORMAC INC <br /> Site facility address: 6215 TAM 0 SHANTER STOCKTON <br /> RB LUSTIS Case :No: Local Case No: LOP Case No: 1258 <br /> URF filing date: 08/10/89 SWEEPS No: <br /> Responsible Parties Addresses Phone Numbers <br /> NORMAL INC 3449 LONGVIEW (916) 482-7924 <br /> NORTH HIGHLANDS CA 95660 <br /> Tank No Size in Gal. Contents Closed in-Place/Removed? Date <br /> 1 11000 UNLEADED GAS REMOVED 07/12/89 <br /> 2 <br /> i <br /> 3 <br /> III. Release and Site Characterization Information <br /> Cause and type of release: UNAUTHORIZED <br /> Site characterization complete? (Yes) No Date approved by oversight agency:12/12/95 <br /> Monitoring wells Installed? (Yes) No Number:3 Proper screen interval? (Yes) No <br /> Highest GW depth below ground surface: 35' Lowest depth: 60, Flow direction: Sw <br /> Most Sensitive, Current Use: BENEFICIAL <br /> Are drinking water wells affected? Yes (No) Aquifer name:CENTRAL VALLEY REGION 5 <br /> Is surface water affected? Yes 71go) <br /> Nearest/affected SW name: <br /> Off-site beneficial use impacts (addresses/locations) : N/A <br /> Report(s) on file? (Yes) No Where is report(s) filed? PHS/EHD <br /> i <br /> Treatment and Disposal of Affected Material <br /> Material Amt. (inc. Units) Action (Treatment or Disposal w/Destination Date <br /> Tank . 1,000 GALLON THORPE OIL,SCRAPED IN LODI 07/12/89 <br /> Piping ABOVE TANK 3 FEET THORPE OIL,SCRAPED IN LODI 07/12/89 <br /> Free Product N/A <br /> Soil 550 YD AERATED ON SITE 01/19/90 <br /> Groundwater N/A N/A <br /> Barrels N/A N/A i <br /> f F <br /> - Exhibit N Page 1 of 2 <br />
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