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REG 603 UPDATE-8 7/17/92 <br /> • <br /> Involved regulatory agencies suggested that product recovery <br /> commence before an aquifer pump test be performed <br /> Temporary submersible pneumatic pumps were installed into monitor <br /> wells MW-1 and MW-3 for product recovery on October 10, 1989. <br /> Approximatell 40 gallons of gasoline was recovered. The product <br /> recovery system was removed in February, 1990, and the "ConVault" <br /> tank, until September, 1990, was being used for the storage of the <br /> purged well water. On May 25, 1990 a water sample obtained from <br /> the "ConVault" indicated that the stored water was free of <br /> petroleum hydrocarbons (Table 1 Convault) . This water was later <br /> dumped to the sewer after permission was obtained by the Stockton <br /> Department of Municipal Utilities (approximately 250 gallons) . <br /> During the November 27, 1990 monitoring round, 0.08, of a clear <br /> yellow floating product was again discovered in monitor well MW1 <br /> This well was purged until depletion of the product was noted; <br /> approximately 1 quart of gasoline was recovered and placed into <br /> the 55 gallon drum storing the water "purged" prior to sampling <br /> the wells. Product thickness measurements obtained on subsequent <br /> site visits have shown only a sheen of product in MWl until <br /> September, 1991 when 0.02 feet of yellow-amber product was <br /> . discovered, and also wells MW3 has had up to 0.28 feet of yellow- <br /> amber product and MW10 have product sheens (showing up after the <br /> commencement of the vapor extraction source test on MW10 and the <br /> continuation of vapor extraction on MW1, MW2, MW3, MW10 and the <br /> tanks excavation area) <br /> 3.2 SITE CONDITIONS <br /> A. GROUND WATER <br /> A. 1 GROUND WATER March 10, 1992 <br /> The March, 1992 chemical results (sampled 3/10/92) indicate <br /> that dissolved benzene in monitor wells MW-2, MW-4 and MW-8 <br /> substantially exceeds the action level for drinking water of 1 0 <br /> ppb, set by the DHS, see Table 1. Monitor wells MW-6 and MW-9 <br /> have low levels of benzene (1.3 and 4 3 ppb respectively) and <br /> Monitor wells MW-5 and MW-7 are below the detection limit (<0.3) <br /> for benzene. Since the start up of vacuum Pxtraction from MW1 and <br /> MW10 the benzene levels in the monitor wells have dropped in all <br /> of the wells, see Figures 5A and 5B and Table 1 Monitoring wells <br /> MW2 and MW3 were added to the vapor extraction system on January <br /> 14, 1992 These wells are influencing the down gradient off site <br /> extent of the plume (MW7 and MWS) . Monitoring wells MW1, MW3 and <br /> MW10 contained floating proauct. Strang to moderate bio-odors <br /> were also noted along with a grey green coloration of the purged <br /> ground water from monitor wells MW2, MW4, MW7 and MW8 <br /> i <br /> PAGE 5 <br />