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y,. Report:Groundwater-quality Monitoring—January 26 2004: 7500 West Eleventh Street, Tracy, CA, Page 13 <br /> The pump inlet was attached to a flexible, transparent, 0.5-in diameter, plastic suction <br /> pipe. This permits the condition of the pumped fluid to be observed. The pump suction <br /> hose was connected to a 0.5-in diameter, 10-ft. long piece of rigid plastic pipe, or lance, <br /> which was lowered into the well until its tip was immersed below the surface of the <br /> floating product, but not to a depth significantly greater than the interface between <br /> groundwater and the floating product. The suction pipe and lance assembly includes a <br /> -b,„ regulating/shut off valve. The pump discharge line is also made from flexible, <br /> transparent, 0.5-in diameter plastic pipe. The discharge pipe directs the recovered product <br /> into the 55-gallon drum that is staged at the well head. <br /> Note: <br /> The purging of Well MW-7 that occurred on January 26, 2004 was <br /> conducted using the standard procedure described in Section 2.2 for purging <br /> wells at the 7500 West Eleventh Street site that is used preparatory to <br /> conducting a round of groundwater-quality monitoring. <br /> 3.3 Floating Product Removed to Date <br /> Since the first round of purging of floating product from Monitoring Well MW-7 <br /> occurred on November 8, 2003, when, prior to purging, the thickness of floating product <br /> in the well was 0.58 ft., five additional purgings of LNAPL from that well have been <br /> performed: November 15, November 22 and December 21, 2003 and January 26 and <br /> March 30, 2004. By November 22, 2003, no floating product was measurable on the <br /> I.-W groundwater prior to its being purged and no more than a sheen was observed on the <br /> extracted groundwater. After a delay of one month, less than one ounce of LNAPL was <br /> recovered from the well when it was again purged on December 21, 2003. Records of <br /> thicknesses of LNAPL that have been measured in Monitoring Well MW-7 are recorded <br /> in Table 3. <br /> As is described above, initially, floating product from Monitoring Well MW-7 was <br /> purged on a weekly basis. However, since a significant thickness of floating product <br /> failed to reappear in the well seven days after the November 15, 2003 purging, to achieve <br /> L a cost-effective operation, SJC reduced the purging frequency to once per month and, on <br /> December 21, 2003, to a quarterly frequency <br /> 3.4 Evaluation of LNAPL Removed from Monitoring Well MW-7 Compared to <br /> Estimated Volume in Subsurface <br /> +- It is instructive to review the results of the LNAPL-purging rounds that have been <br /> completed to date in the context of the likely effectiveness of that interim measure to <br /> influence significantly the mass of LNAPL present in the subsurface beneath the site. <br /> If it is assumed that the porosity of the Monterey sand filter pack around the slotted 2-in.- <br /> diameter casing of Monitoring Well MW-7 is 0.3, given the measured thickness of 0.58 <br /> ~- ft., then the total volume of floating product in the boring on November 8, 2003, <br /> b amounted to 0.07 ft3 (i.e., 0.52 gal.), which is the sum of the LNAPL in the casing itself <br /> A. sic <br />