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SU0005344
Environmental Health - Public
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SU0005344
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Last modified
11/2/2020 10:05:00 AM
Creation date
9/9/2019 11:11:09 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2600 - Land Use Program
RECORD_ID
SU0005344
PE
2627
FACILITY_NAME
PA-0500531
STREET_NUMBER
4620
Direction
E
STREET_NAME
WOODBRIDGE
STREET_TYPE
RD
City
ACAMPO
APN
01709002
ENTERED_DATE
8/26/2005 12:00:00 AM
SITE_LOCATION
4620 E WOODBRIDGE RD
RECEIVED_DATE
8/26/2005 12:00:00 AM
P_LOCATION
99
P_DISTRICT
004
QC Status
Approved
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FilePath
\MIGRATIONS\W\WOODBRIDGE\4620\PA-0500531_PA-0300206\SU0005344\PUB REC REL APPL.PDF
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VFW <br /> INFORMATION SHEET <br /> ORDER NO. R5-2003-0099 <br /> NEWPORT PACIFIC CAPITAL COMPANY <br /> ARBOR MOBILE HOME PARK WASTEWATER TREATMENT FACILTY <br /> SAN JOAQUIN COUNTY <br /> Introduction <br /> Arbor Mobile Home Park(MHP)is at 19690 N. Highway 99 Acampo. Wastewater originates from <br /> residential sources consisting of 173 mobile homes, the nearby Arbor Storage Complex, and a <br /> clubhouse. The MHP is completely occupied, therefore wastewater flow rates are anticipated to <br /> remain stable in the future. The present discharge flow rate is approximately 45,000 gallons per day. <br /> Wastewater System <br /> Raw sewage is collected in the collection system and conveyed by gravity to the wastewater treatment <br /> plant. The Arbor MHP wastewater treatment plant is an activated sludge package plant. Wastewater is <br /> discharged from the package plant to polishing tanks then is disposed of in seepage pits or gravelless <br /> leachfields. There are a total of 60 seepage pits and one gravelless leachfield area. Seepage pits and <br /> the leachfield are rotated between resting and in-service on a regular basis. <br /> Wasted sludge is discharged to the sludge storage tank where it is aerobically digested. The digested <br /> sludge is hauled to the City of Lodi regional wastewater treatment system as needed. <br /> The seepage pits are 60-inches in diameter and 25-feet deep with a perforated PVC pipe positioned in <br /> the center of each well. The pipe is positioned in the center of each well with crushed rock packed <br /> around the pipe and on the bottom of the well. The unsaturated zone between the bottom of each well <br /> and the shallowest reported groundwater level is approximately 25 feet. <br /> The Discharger has experienced failure in the disposal area due to high concentrations of suspended <br /> solids in the effluent, which resulted in reduced permeability and reduced infiltration. In response to <br /> the failure, the Discharger has improved operation of the system to reduce the concentration of <br /> suspended solids in the effluent. This Order requires the Discharger to prepare an Operation and <br /> Maintenance Plan, an Effluent Collection System Plan, a Groundwater Well Installation Workplan, a <br /> Groundwater Well Installation Report, and a Groundwater Quality Study Report. <br /> Effluent Limitations <br /> Effluent limitations are included in the WDRs. The limits address total dissolved solids (TDS), total <br /> suspended solids (TSS), and biochemical oxygen demand (BOD). The limits were included to allow <br /> the Discharger to continue operation of the wastewater treatment system while groundwater quality <br /> data is collected. The effluent limits were selected based on the treated wastewater concentrations. <br /> Total Dissolved Solids <br /> The TDS limitation is based on TDS concentrations in the water supply and treated wastewater. The <br /> use of the water by residents results in a TDS concentration increase of approximately 125 mg/L. The <br /> limit was set at 400 mg/L (monthly average) and 600 mg/L (daily maximum)based on two sample <br />
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