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SUBNUT IN DUPLICATE ! IViSION OF OIL AND GAS
<br /> R=QURC8:aACWCYOICALIIORNIA ; a ��'Vr
<br /> DVARTMCNT OI CONSMVATION Rte.0
<br /> DIVISION OF OIL AND GAS MAY 2 8 1991
<br /> History of Oil or Gas Well 11/000LAND,CALIFORNIA
<br /> Operator .,,Quintana Petroleum,Corporation,,,,,,,,,Field County ...San.,Joag4IR
<br /> Well......... PIACENTINIE #1...27.. ............ . , Sec.. .2L, T... N...., R ..5.9. . ,.NP.,B. & M.
<br /> A.P.I. No...04-077.-20484......................... Name....J�...M�...$nod-r.......................... Title
<br /> .
<br /> Date .........MaY... .1................ . 19.7Q.1., (PenonsubmtttingreponI (Ptaldest.SmatmatAssm)
<br /> Signature........... :.. .. .............
<br /> 1325So. Colorado Blvd.,., Suite. 4.1.1 t Denver=, CO. 8022,2 ,,, ....U0,5)M79559....
<br /> (Address) (Telephone Number)
<br /> History must be complete in all detail. Use this form to report all operations during drifting and teasing of the weIl or during redrilling
<br /> or altering the casing,plugging,or abandonment with the dates thereof.Include such items as hole size,formation teat details,amounts
<br /> of cement used, top and bottom of plugs,perforation details,sidetracked jurd; bailing tub aid initial production data.
<br /> Date
<br /> Workover - AFE 051006
<br /> Purpose: Recomplete to shallower zone within Mokelumne Sand.
<br /> 5/7/91 4856' Day 1. RD flowline and equipment. Prep to MI WO rig.
<br /> DC $1179 CTD ;1179
<br /> 5/8/91 4856' Day 2. MW 9.4 MI RU Snow Oilfield Service Rig O8. RU lines. PI
<br /> and killed well w/40 bbls 9.4 ppg brine water. Well on vacuum.
<br /> ND tree. NU BOP's. Tested BOP's. Release packer and POOH. RU
<br /> wireline. Ran gauge ring and junk basket to 4740'. WIII w/EZSV
<br /> and set at 4730'. Closed BR and tested casing and retainer to
<br /> 1000 psi. SWIFN.
<br /> DC $6523 CTD $7702
<br /> 5/9/91 4730' Day 3. MW 8.8 TIH w/stinger. Teat retainer on casing to 1000 psi.
<br /> Mixed 50 axe Class "G" cement at 15.8 ppg. Squeezed perforations
<br /> 4750'-4764' at final rate of 1/2 bpm 2600 psi, 1500 psi static.
<br /> Reversed out 5 axe cement. POOH. GIH w/production tubing. Set
<br /> packer at 4611'. Tested pkr to 1000 psi. ND BOP!:a. NU tree. SWIFN.
<br /> DC $7906 CTD ;15,608
<br /> 5/10/91 4730' Swbd wall to 1200'. Perforated 4720'-4724' with 4 japf. RU swab.
<br /> Tagged FL at 12001. Swbd to 25001, well started unloading.
<br /> Cleaned up well. Final flow on 12/64" ck 800 MCFD, FTP 1050 psi.
<br /> No water. SI well. 30 min SIP 1100 psi. RD and release rig.
<br /> DC $6785 CTD ;22,393
<br /> FINAL REPORT
<br /> 5/14/91 Well returned to production 9:00 a.m.
<br /> ���' li ( �I( }�{�,�y)��pr°�'il'1MantihiUn% 11 ,�,It•��1��i3'S�gql�tlsdi i�.°i
<br /> tAlk,Q€if pl�iS'!i,i1 (l 918",Tu6ylp Da{iil')3iss=s:,,1,i'83�rt IllgfSsbt .
<br /> ilt�r 1} lrY1F,r t3:s( r r`
<br /> 1 1718'MULESHOE .88
<br /> 1 S 112•BAKER MODEL R DOUBLE ORIF PKR 7.18
<br /> 11T 2 7/8'6.5M 1.55 BUS TUBING 31.14
<br /> 1 2 7/8'F NIPPLE(I.D.2.31') .97
<br /> 149 JTS 2 718'6.S#I-SS DUE TUBING 4,557,42
<br /> 1 2 718'TUBING HANGER .80
<br /> TOTAL TUBING AND EQUIPMENT 4,598.39
<br /> DISTANCE RKB TO HANGER +13.00
<br /> yaaaEFFECTIVE TUBING 387MNO 4,611.39
<br /> �}�4i
<br /> i' , 311
<br /> OG103(3/ee/DWAR/5M)
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