Laserfiche WebLink
' •-1 Cn CO. /OiW MO .N• <br /> 4. <br /> 1, <br /> QUINTANA PETROLEUM CORPORATION SHEET D <br /> DRILLING RECORD PAGE NO. 2 <br /> AFE 1156603 <br /> LEASE PIACENTINF WELL NO. 1-27 FIELD <br /> DATE --YJAR� AI Or OPERATIONS, ON LT <br /> PBTD <br /> 7/22/86 4856' Day 1. MIRU Weltech Rig 11246. NU BOPE and tested to 2000 psi, TIH w/bit <br /> and scraper. Tagged cmt top at 48461. RU swivel and drld cmt stringers <br /> to 48560, SDFN. <br /> DC: $11,951 CTD: $147,756 <br /> 7/23/86 4856' Day 2. Circ out w/9.4 ppg brine. POOH w/bit and scraper. RU Welex. <br /> Press test lubricator to 2000 psi, TIH w/4" csg gun and perf Mokelumne Sd <br /> from 4149'-63' w/8 JSPF (CET 7/18/86) - 4750'-64' (LDT/CNL). RD Welex. <br /> RIH w/Baker R-3 pkr and "F" nipple and tbg setting, set pkr at 4702' <br /> w/120011. ND BOPE, NU tree. RU swab equip, tag fluid at 100' down. Pulled <br /> from 1200', well came in and flowed 31 BW to rig tank. Well clean, SIFN. <br /> DCi $25,288 CTD: $173,044 <br /> 7/24/86 4856' Day 3. RDMO rig. RU tester, SITP 1850 psi. Opened well and tested on <br />� . 5 MMCFPD rate for 4 hre. Attempted to raise rate to 10 MMCFPD, separate <br /> burst plate blew. Working on test separator. SITP 1850 psi. <br /> DC: $6680 CTD: $179,724 <br /> 7/25/86 4856' Day 4. Flowed well at t10 MMCFD and 1635 paig tbg press for 4 hours. <br /> SI well - press immediately built to 1860 prig. After 35 min SITP 1848 psig. <br /> Prod .1 bbl wtr (chlorides - 49,000 ppm). Will pull bombe at 1100 hrs today. <br /> DC: $8,000 CTD: $187,724 FINAL REPORT. <br /> 7/28/86 Correction to final cost to date: $220,415 <br /> r <br /> i <br /> i <br /> i <br /> i <br /> I <br /> h <br /> I <br /> i <br /> i <br />