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r <br /> OUINTANA PETROLEUM CORPORATION SHEET D <br /> DRILLING RECORD CONFIDENTIAL <br /> PAGE NO, 1 <br /> :1 <br /> AFE 056622 <br /> LEASE 9ROV ' I WELL NO. 1-8 FIELD <br /> A DtTAILS Or optRATIONS. DESCRIPTION{ Y RCb <br /> Location: 1200' FEL 6 600' FSL <br /> NE :.•W NW Section 8, T4N-R6E <br /> San Joaquin County, California <br /> 10/22/86 MIRU Gary Drilling Rig #16. Expect to spud 10/23/86. ~� <br /> 10/23/86 RU Gary Rig #16. Expect to spud this afternoon. <br /> 10/24/86 535' Day 1. Drld 495' WOC, <br /> clay and sd, MW 9,8, vis 40, WL 10.5. <br /> 1° @ 260' . V @ 535'. SPUD at 1600 hrs 10/23/86. Drld to 535'Surveys: <br /> , made <br /> clean up trip to surf, POOH. Ran 13 jts 2411 csg, set at 534.151. Cmt <br /> using BJ Titan w/131 sx Class G + 8% gel, 37. CaC12, followed by 100 ax <br /> G + 3% CnCl2/ Total volume 354 cu ft. Displace w/180 cu ft mud. <br /> Bump plug w/1000 pis. Release press, float held. CIP at 0245 hrs 10/24/86. <br /> Had 50 cu ft clean cmt returns. WOC 6 hrs, cut off csg, install csg head, 1. <br /> NU BOPE. DC: $5028 CTD: $21,986 <br /> 10/25/86 1671' Day 2. Drld 1136' , drlg, ss, clay, sd, MW 9,2, via 38, WL 10.2. <br /> Durvey: 1° @ 1205', Fin WOC. Weld and test csg head to 700 psi. NU <br /> and test BOPE to 1500 psi and annular to 1000 psi. Witnessed by Hike <br /> Cummings w/D,O.G, NDA at 16711, <br /> DC: $20,863 CTD: $42,669 <br /> 10/26/86 3865' Day 3. Drld 2194', drlg, sd and clay, MW 9,6, vis 40, WL 7.9. Surveys: <br /> k° @ 1948', 1* <br /> @ 2690', V @ 3156'. Drld to 31561, TFB 02, NDA at 3865'. 1' <br /> DC: $8010 CTD: $50,679 V� <br /> 10/27/86 4400' Da 4, <br /> 2°y@ Drld <br /> WOO , sd and clay, MW 9.6, vis 39, WL 7.8. Surveys: <br /> Drld to 3928' , wipe hole, drl to 44001, wipe <br /> hole, circ and cond, TOOH, Log, <br /> DC: $12,575 CTD: $63,254 <br /> 10/28/86 TD 4400' Day 5. WOO, LS DC. TIH OE and plug well as follows: <br /> Plug #1: 1765'-1365' w/118 sx "G" + 3% CaC12 <br /> Plug 02: 586'- 486' w/ 60 sx "G" + 37. CaCl <br /> Plug #3: 518'- 450' w/ 30 sx "G" + 2 <br /> 3 <br /> Plug 114: 30'-surf w 3% a <br /> CaC12 <br /> LD DP, ND BOPE, cut off wellhead, clean mud tanks. Rig released <br /> at 0400 hrs 10/28/86. Well plugged and abandoned. FINAL REPORT. i. <br /> DC: $21,230 CTD: $84,521 Ki.. <br /> 8 5/8" CASING DETAIL _ <br /> 10/24/86 <br /> 1 8 5/8" Baker guide shoe <br /> 1 jt 8 5/8" 24/l K- 1.04' <br /> 55 8Rd ST&C R-3 Casing 42.12' <br /> 1 - 8 5/8" Insert . . "' <br /> 12 jts 8 5/8" 2411 K-55 8Rd ST&C R- 0.00' <br /> 3 Casing "' 495.51' l <br /> Total casing run <br /> Casing cut off 538.61' <br /> Casing in hole . , .... ����"���' <br /> 17.02' <br /> RKB to C11F 521.6 ;y <br /> Casing set at .................................. +12.50' <br /> 534.15r <br /> r1 <br /> r:. <br /> �i <br />