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NP-1-80',NP-1-90',SVE-South and SVE-North are consistent with previous sampling events <br /> (see Table 4). <br /> Concentrations detected in MW-DIS-1 during this monitoring event were higher than those <br /> in February 1999. TPH as gasoline was detected in MW-DIS-1 at a concentration of 6,800 <br /> µg/L and benzene,toluene, ethylbenzene,and total xylenes were detected concentrations of <br /> 440,450,280,and 1,200�tg/L, respectively. <br /> i . <br /> Oxygenates <br /> Methyl-tert-Butyl Ether (MTBE), tert-Butanol(TBA),Di-isopropyl ether (RIPE), Ethyl-tert- <br /> butyl ether(ETBE),and tert-Amyl Methyl ether(TAME)were not detected in any of the <br /> wells during this monitoring event. All oxygenates were analyzed by EPA Method 8260 <br /> during this sampling event. <br /> There have been no confirmed detections of the MTBE,DIPE,ETBE, and TAME at this site. <br /> TBA has been detected once,in five different wells,but has not been detected in any well <br /> during the past four to five consecutive sampling events. <br /> Conclusions <br /> Since 1991,groundwater levels have risen approximately 30 feet(from 77 ft bgs to 47 ft bgs), <br /> and the direction of groundwater flow has changed directions by almost 180 degrees. <br /> Between 1991 and July 1994,the groundwater flow direction was predominantly towards <br /> the northwest at an average groundwater flow direction and magnitude of 312° and 0.0006 <br /> ft/ft. From October 1995, through today, the groundwater flow direction has been <br /> consistently towards the southeast,at an average direction and magnitude of 143°and <br /> 0.0008 ft/ft. The groundwater flow direction has been toward the southeast for the past 12 <br /> sampling events,indicating a stable flow regime. Due to the switch in flow directions, <br /> previous downgradient wells are now upgradient wells. <br /> Prior to the switch in groundwater flow directions, the extent of the plume was defined <br /> horizontally by monitoring wells MW-DIS-3,MW-DIS-8S,MW-DIS-9,and MW-DIS-10.The <br /> vertical extent downgradient of the source area was defined by monitoring well <br /> MW-DIS-8D. Currently,the extent of the plume in the southeast direction is unknown. <br /> Analytical results from all wells at the site have been extremely consistent,with the <br /> exception of monitoring wells MW-DIS-1 and-2,which have had significant reductions in <br /> concentrations of petroleum hydrocarbons. <br /> There have been no confirmed detections of gasoline additives or oxygenates at this site. <br /> Tert-butanol(TBA)has been detected a single time in five different wells.TBA was detected <br /> in monitoring wells NP-1-70',NP-1-90',and SVE-North on December 23, 1997. TBA has not <br /> detected in any of these wells during the past five consecutive sampling events.TBA was <br /> detected in monitoring wells MW-DIS-1,and SVE-South on May 21, 1998. TBA has not been <br /> detected in these wells during the past four consecutive sampling events.The Disco tanks <br /> were in operation between 1966 and 1976. MTBE was first used as an octane booster in the <br /> mid-1980's,and widespread use began in the 1990-1992 period in order to meet air quality <br /> requirements.Therefore,it is highly unlikely that the gasoline released from the Disco site <br /> 1 contained any additives or oxygenates. <br /> r <br /> 3 <br />