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ARCHIVED REPORTS_XR0009426
Environmental Health - Public
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3500 - Local Oversight Program
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PR0545053
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ARCHIVED REPORTS_XR0009426
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Last modified
12/11/2019 11:12:37 AM
Creation date
12/11/2019 9:48:50 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0009426
RECORD_ID
PR0545053
PE
3528
FACILITY_ID
FA0005720
FACILITY_NAME
SMITH CANAL PUMP STATION
STREET_NUMBER
2130
STREET_NAME
FONTANA
STREET_TYPE
DR
City
STOCKTON
Zip
95204
CURRENT_STATUS
02
SITE_LOCATION
2130 FONTANA DR
P_LOCATION
01
P_DISTRICT
003
QC Status
Approved
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EHD - Public
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f;r A S S O C I A T E S I N C . <br /> ?, In Jul 1999 ATC conducted a groundwater extraction test. The aquifer test was conducted over <br /> Y � g q <br /> a 24-hour period by extracting groundwater at a constant rate from well MW-4. The test was <br /> performed to determine the aquifer properties and the radius of influence for groundwater <br /> pumping. <br /> The groundwater pumping rate during the pilot test, as measured by the flow meter, averaged <br /> approximately 3 gallons per minute (gpm)for the first half of the test and 5.5 gpm for the second half <br /> M of the test. The collected data were analyzed using AQTESOLVTm groundwater modeling software <br /> and a recovery test analysis. <br /> The observed maximum drawdown in each of the four observation wells during the test was <br /> plotted against the distance of each well from well MW-4. Based on the observed data, the radius <br /> of influence for groundwater extraction at the site is greater than 50 feet. Observation well MW- <br /> 1 is located approximately 46 feet from pumping well MW-4 and the groundwater elevation <br /> dropped about 1.7 feet in this well. Observation wells MW-2, MW-3, and MW-5 are each <br /> located approximately 55 feet from pumping well MW-4 and the groundwater elevation dropped <br /> 1 about 0.7 feet in each of these wells. In general, a small radius of influence is expected for <br /> pumping in an unconfined aquifer. <br /> The Cooper-Jacob type-curve solution for an unconfined aquifer was used to estimate aquifer <br /> eters. The obtained results for the story using the Cooper-Jacob a coefficient <br /> Param g g solution were a <br /> little lower than expected for an unconfined aquifer. The storage coefficients for unconfined <br /> aquifers are typically between 0.01 and 0.3, while those for confined aquifers are typically between <br /> 0.00005 and 0.005 (Driscoll page 210, 1986). The average storage coefficient calculated using the <br /> Cooper-Jacob solution was 0.0015. Although the storage coefficients were lower than expected, <br /> <_ this method was considered appropriate for the site conditions. <br /> The average hydraulic conductivity values (0.001 meters per second [m/s]) calculated fall within <br /> e_-r <br /> =:r the average range for fine to coarse sand (1 to 10'S m/s) (Driscoll page 74, 1986). <br /> Using this hydraulic conductivity, an average groundwater velocity can be calculated. Based on <br /> an average groundwater gradient of 0.0077, the average groundwater velocity is approximately <br /> 1.66 meters/day or almost 2,000 feet per year. This is an average velocity but is not necessarily <br /> �I,' representative of the movement of the TPHd plume because it does not take into consideration <br /> effectsavec=ion ispersion;a_r anis ropic and/or non us geology. The plume of <br /> TPHd appears to be migrating at a much slower rate as the elevated concentrations historically <br /> detected in well MW4 have not been observed in hydraulically downgradient wells MW2 and <br /> MW3 since monitoring began in 1989. <br /> 4.2.2 Petroleum Hydrocarbons in Groundwater <br /> Total Petroleum Hydrocarbons as diesel have historically have been detected in the greatest <br /> concentrations at monitoring which is adjacent to the former UST. This monitoring <br /> g well MW4� J g <br /> w:162574.021repor \closure-smith.doc 5 <br /> 2 <br />
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