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WORK PLANS_FILE 1
Environmental Health - Public
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3500 - Local Oversight Program
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PR0545275
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WORK PLANS_FILE 1
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Last modified
2/3/2020 2:01:36 PM
Creation date
2/3/2020 12:24:01 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
WORK PLANS
FileName_PostFix
FILE 1
RECORD_ID
PR0545275
PE
3528
FACILITY_ID
FA0005678
FACILITY_NAME
LATHROP SHELL
STREET_NUMBER
16500
Direction
S
STREET_NAME
HARLAN
STREET_TYPE
RD
City
LATHROP
Zip
95330
CURRENT_STATUS
02
SITE_LOCATION
16500 S HARLAN RD
P_LOCATION
07
P_DISTRICT
003
QC Status
Approved
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h <br /> Remedial Action Plan-Tosco 76 Branded Facility No. 11195 <br /> June 21, 1999 <br /> transportation was performed by WMIS. The water was transported to the Tosca Refinery for <br /> disposal. A total of approximately 102,760 gallons of groundwater were removed from the former <br /> and present UST pits and transported to the Tosco Refinery between January 1999 and March 26, <br /> 1999. <br /> The groundwater wells Dave been monitored and samples on a quarterly or semi-annual to basis <br /> since 1993. The most recently collected groundwater samples, collected on March 22, 1999, <br /> contained petroleum hydrocarbons at concentrations ranging from not detected to 65,000 ppb (MW- <br /> 5) of TPHg, not detected to 95,000 ppb (MW-5) of MtBE, and not detected for benzene. Depth to <br /> water has historically ranged between approximately 6 to 12 feet below top of casing (TOC). The <br /> groundwater flow direction has ranged from southeast to southwest with an average gradient of <br /> 0.001 feet/feet or less (Alisto, 1999; Blaine Tech Services, Fourth Quarter 1998 Groundwater <br /> Monitoring Report, dated May 1999; and BP letter to the SJCEHD, dated May 3, 1999). <br /> DISCUSSION OF RECENT FIELD WORK AND ANALYTICAL RESULTS <br /> On April 9, 1999, GR personnel witnessed the removal of approximately 5,000 gallons of <br /> groundwater from the former UST backfill utilizing the conductor casing. The groundwater was <br /> pumped into a 5,000-gallon vacuum truck by WMIS and transported to the Tosco Refinery for <br /> disposal. After groundwater removal, a water sample, labeled CC-1, was collected from the <br /> conductor casing. <br /> Groundwater sample CC-1 was submitted to Sequoia Analytical (Sequoia), in Walnut Creek, <br /> California (ELAP #/1271), where it was analyzed for TPHg, BTEX, and MtBE. The sample <br /> contained 5.3 ppb of benzene, 6,300 ppb of MtBE, and was reported as not detected for all other <br /> analytes. Groundwater sample analytical methods and data are summarized in Table 1. Copies of <br /> the laboratory reports are attached. <br /> In conjunction with the April 9, 1999 groundwater purging and sampling, GR conducted a <br /> performance test to qualitatively analyze of the radius of influence generated during removal of <br /> 5,000 gallons of groundwater from the conductor casing. During pumping, GR personnel collected <br /> depth to water (DTW) readings from the conductor casing and on-site monitoring wells MW-3, <br /> MW-4, and MW-6 (Figure 2). These wells were used as observation wells. DTW readings were <br /> collected continuously, beginning prior to initiation of groundwater pumping until 125 minutes after <br /> completion of pumping activities, for a cumulative total of 160 minutes. The conductor casing was <br /> purged for 35 minutes to fill the 5,000-gallon vacuum truck, at which time the casing was beginning <br /> to dewater. The maximum observed drawdown in the conductor casing was 1.92 feet. Observation <br /> well MW-3, located approximately 45 feet from the conductor casing, showed a drawdown of <br /> approximately 0.70 feet after 55 minutes. Drawdown in observation well MW-4, located <br /> approximately 8 feet from the conductor casing, was approximately 0.38 feet after 40 minutes. <br /> Observation well MW-6, located approximately 114 feet from the conductor casing, showed a <br /> drawdown approximately 0.20 feet after 75 minutes. Groundwater drawdown data are summarized <br /> in Table 2. <br /> 140193.07-1 <br /> 4 <br />
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