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Site History <br /> Boyett Petroleum(419 S.Main St.,Manteca) <br /> 1Page 2of9 <br /> intervals for soil classification and three soil samples were collected from each boring at depth intervals <br /> of 16-16.5 feet, 20-21.5 feet, and 26-26.5 feet for laboratory analyses. Laboratory analytical results of the <br /> twelve soil samples indicated petroleum hydrocarbons were not detected at or above the laboratory <br /> reported detection limits in any of the samples. <br />' On February 2, 2001, WHF, in conjunction with VBI In-Situ Testing of Sacramento, California, advanced <br /> two CPT borings at the site. CPT-1 and CPT-2 were completed to depths of 76 and 76.4 feet bgs, <br /> respectively. Both borings were terminated due to refusal. Beds of clay were encountered in CPT-1 at <br />' depths of 20 to 24.1 feet and 50.2 to 57.6 feet bgs. In CPT-2, beds of clay were encountered at depths of <br /> 23.8 to 26.4 feet, 49.7 to 56.4 feet, and 62.7 to 66.9 feet bgs. WHF submitted a report of their findings of <br /> the CPT borings in a letter dated February 7, 2001, to Mr. Jeffrey Wong of the SJCEHD. <br />' On April 25, 2001, WHF, in conjunction with Frontier Drilling, completed a deep monitor well, MW-9, <br /> to a depth of 50.5 feet bgs. The screened interval for the well was installed at approximately 40.5 to 50.5 <br /> feet bgs. Groundwater depth was measured at approximately 17 feet bgs. Two soil samples were collected <br /> from the borehole at depths of 43.5 feet and 50 feet for laboratory analyses. None of the analytes of <br /> concern (BTEX, TPH-G, and MTBE) were detected in the soil samples collected from the borehole of <br /> MW-9. Laboratory analytical results of a groundwater sample collected from MW-9 indicated that none <br /> of the analytes of concern (BTEX, TPH-G, and selected gasoline oxygenates/additives) were detected, <br /> with the exception of MTBE, which was detected at a concentration of 14 4g/L. In the Final Report of <br /> Findings —Lateral Extent of Groundwater Contamination dated June 29, 2001, WHF concluded that the <br />' source of the petroleum hydrocarbon contamination had not been identified and recommended that <br /> quarterly groundwater monitoring continue, one additional monitor well be installed directly east of the <br /> fuel island, and that no remedial action be taken at this site until the source was identified. <br />' . On September 26, 2002, a representative of Condor was onsite to measure water levels and collect <br /> groundwater samples at monitor wells MW-I through MW-9 for the third quarter 2002 groundwater <br /> monitoring event. Monitor wells MW-4, MW-5, and MW-6 were heavily silted, and MW-4 and MW-5 <br /> were dry. Mr. Jeffrey Wong of the SJCEHD was onsite to observe a portion of the field activities. <br /> At the request of the SJCEHD, a Condor representative was onsite to redevelop monitor wells MW-4, <br /> ' MW-5, and MW-6 on September 27, 2002. The redevelopment procedure applied to MW-4 and MW-5 <br /> consisted of flushing the wells with potable water, and then bailing the water from the wells. The <br /> sediment removed from the wells consisted of medium to coarse-grained, well-rounded, and well-sorted <br /> sand. The redevelopment activities failed to significantly reduce the amount of sediment inside the well <br /> casings; consequently, redevelopment of MW-4 and MW-5 was not successful. Based on Condor's field <br /> observations, it appeared the casings of these wells are damaged and allowing the annular sand pack to <br /> ' infiltrate inside the casings. MW-6 was successfully redeveloped by removing a significant amount of the <br /> sediment from inside the well casing. A groundwater sample was collected for laboratory analyses from <br /> MW-6 on September 30, 2002. No floating product, sheen, or odors associated with petroleum <br /> hydrocarbons were observed in any of the wells sampled during the third quarter 2002 quarterly' <br /> ' groundwater monitoring event. All of the groundwater monitor wells sampled contained a significant <br /> amount of suspended sediment. Laboratory analytical results for the groundwater samples collected at the <br /> site on September 26 and 30, 2002, indicated that none of the analytes of concern (BTEX, TPH-G, and <br /> ' selected gasoline oxygenates/additives) were detected at or above the laboratory reported detection limits <br /> in the groundwater samples collected from MW-3, MW-6, and MW-8. MTBE was detected in the <br /> �..7.. atct r n ,,.-ples --c!lecte 7 4',-n.+., A/IY-1 M'%V_'7 N!'% 1 '7 an 1111111-1117-19. 'r AAAA A»ac raPtPr�Ynrl .T 4 ,- <br /> 1 V Ul�\a�Y LL�41 .�uiai <br /> L+ �livJ vvaivv�vaa as va.a a.i �. a, iri r� r, ira rr i, uaau a.�..a.� ...... .+�..—� �» ... ...� <br /> groundwater samples collected from MW-1 and MW-7. Static water level measurements collected on <br /> September 26, 2002, generally indicated a groundwater flow direction to the south/southwest. <br />