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Gcolagual recluucslnc Page 11 <br /> Dual Phase Extraction Pilot Test Report <br /> Project No 662 2 <br /> February 22,2005 <br /> tproperly and recorded readings as "December 30, 1899" (see Appendix D for Barologger® <br /> data table printout) We called Solinst and confirmed the unit malfunctioned and the data <br /> ' recorded was unusable <br /> A second problem occurred with heavy rain fall during the test The Levelogger in MW-1 <br /> ' was removed because rain water was flowing into the well box and seeping into the well <br /> The wells have to be open for the Leveloggers to function properly but MW-1 was sealed as <br /> soon as the water infiltration condition was discovered All of the Levelogger graphs are <br /> included in Appendix D <br /> A third problem was a malfunction in the MW-6 Levelogger that did not operate correctly <br /> ' and recorded the elevations as the"32 80" foot range of the instrument This data is included <br /> in Appendix D <br /> ' In spite of the inability to compensate the Leveloggers for barometric pressure a graph of the <br /> MW-3 Levelogger data does illustrate groundwater elevations changes GTI produced Figure <br /> ' 4 using the MW-3 elevation data and added notes to show operator induced changes <br /> The calculated groundwater extraction rates from shallow extraction well EW-2 varied 0 8 — <br /> 18 gpm for the first 22 hours of the pumping test This well had an approximate water <br /> column of 5 feet at the start of the test and the decline in extraction rate was expected as the <br /> well dewatered <br /> ' Extraction from EW-2 and the deep extraction well EW-1 commenced on December 7`i' <br /> (Tuesday) at 11 15 The stinger was lowered to the water table (-27 feet bgs) but the hose <br /> 1 continually "deadheaded" as stated above in section 4 3 The stinger was lifted from 27 feet <br /> bgs to 20 and water started flowing again As evident in Table 5, the combined now from the <br /> two wells started at 2 6 gpm and then rose to 11 gpm by 16 00 Figure 4 shows a drop of <br /> ' approximately 0 5 feet when the two wells were active GTI believes that a rate of 10 gpm <br /> could have been sustained throughout the remainder of the test if we had the capacity to store <br /> the water As noted above we had to reduce pumping rates to preclude the American Valley <br /> ' tank from overflowing <br /> Figure 4 shows several increases on Tuesday night as the extraction rate was adjusted to <br /> ' preclude overfilling the American Valley tank Once the water pickup schedule was set at <br /> three events per day the system achieved a fairly consistent 5 — 7 gpm The groundwater <br /> elevation in MW-3 showed a gradual recovery until the system failure on Thursday afternoon <br /> ' The system was restarted at 16 00 and the elevation declined again as extraction continued <br /> One last spike is evident on Friday afternoon as the Mako contractor was showing the <br /> ' equipment to another client (with GTI's permission) and made changes to the system <br /> 1 <br />