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Corrective Action Plan <br /> Prior to the monitoring cell installation, in November 1989, a soil boring designated as B-9 had <br /> been drilled adjacent to the UST Analyses of soil samples collected during the drilling of soil <br /> boring B-9 and the adjacent monitoring well MWA (now BEI-MW3) indicated the soil was <br /> impacted from near the surface to a depth of more than 20 feet bgs The highest concentrations <br /> of TPHg were found at a depth of 15 feet bgs Also, In both borings near the former UST, the <br /> eleN ated TPHg concentrations were evident in samples taken as high as 5 feet bgs This <br /> occurrence indicates the petroleum release may have resulted from a leaking dispenser or piping <br /> most likely located in the immediate vicinity of the UST <br /> The wells installed by Greg Drilling for Blymer were completed at a depth of approximately 30 <br /> feet bgs The water table at the time of well installation was approximately 20 feet bgs The <br /> wells were screened from 15 feet bgs to the bottom Casing size for the Blymer monitoring wells <br /> has been reported at different times as either 2-inch-diameter or 4-inch-diameter Field <br /> observation has shown, however, that they are, in fact, 4-inch-diameter wells The well <br /> construction data for all monitoring wells associated with the site investigations are summarized <br /> in Table 2 <br /> With respect to groundwater gradient and flow direction, monitoring well BEI-MW3 is <br /> considered to be located at the source At various times during the groundwater morutoring <br /> period, well BEI-MW2 has been downgradient and crossgradient BEI-MWI has been both <br /> upgradient and crossgradient of the source <br /> In November 1991, SRK installed three monitoring wells and two test borings The monitonng <br /> wells are designated on the site plan (Figure 2) as SRK-MWI, SRK-MW2, and SRK-MW3, the <br /> test borings as SRK-BH1 and SRK-BH2 During drilling of the wells and test borings, soil <br /> samples collected from depths of 15 feet and 30 feet bgs from each boring were analyzed No <br /> hydrocarbon concentrations were detected in any of the samples (see Table 1) During the time <br /> of drilling, the depth to the water table at the site was approximately 24-25 feet bgs The wells <br /> were completed at depths of 38-39 feet bgs and were screened from 23-24 feet bgs to the bottom <br /> The sand pack in these wells extended approximately 5 feet above the screen The wells were 4- <br /> inch-diameter casing installed in a 10-inch-diameter boring Well construction details are <br /> summarized in Table 2 <br /> With respect to groundwater gradient and flow direction, monitoring wells SRK-MWI and SRK- <br /> MW2 have, at various tunes during the monitoring period (1991 to the present), ranged between <br /> upgradient and crossgradient of the source SRK-MW3 has generally ranged between <br /> crossgradient and upgradient of the source <br /> In April 1996 Park installed two monitoring wells on the Union Pacific Railroad P g ro d property <br /> immediately adjacent and south of the site The wells are designated as MW-7-P and MW-8-P <br /> Their respective locations are illustrated on the site plan (Figure 2) Soil samples collected during <br /> the installation of these wells were analyzed at the depths of 10, 15 and 20 feet bgs Elevated <br /> hydrocarbon concentrations (101 mg/kc, TPHg) were detected in the soil sample collected from <br /> OST <br /> 701-1 cap Page 5 <br />