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• <br /> Site 1: Automotive Service Station, A C-Sparge m unit (Model 3600) was <br /> installed at a gasoline service station The unit was equipped with an oxygen <br /> generator, allowing ozone concentrations to be adjusted between 100 and 300 <br /> ppmv A recurulating well installation was employed to assure adequate ozone <br /> mixing in the vicinity of the monitoring well Dissolved oxygen content and <br /> redox potential (ORP)were monitored to define the radius of influence(ROI) <br /> previous borings on the site showed static groundwater at depths of 3 0 to <br /> 6 0 ft (1 to 18 m) below grade. A brownish-gray silt extended from fill at 2.5 ft <br /> (8 m) to about 6 ft (1 8 m) below grade Medium sand and gravel extended to <br /> depths of 20 ft (6 m) below grade Soil permeability ranged from 10-3 to 10' <br /> cm/sec. The upper soils between 3 5 to 4 0 ft 0 to 12 m)were measured at 9 0 x <br /> le cm/sec with a moisture content of 299 Fine materials (silt and clay) in <br /> smaller fractions (5% or less) were found intermixed with the sand and gravel <br /> The pH of the groundwater was determined to fall in the range of 7 0 to 8 5 <br /> Groundwater flow was low, with a hydraulic gradient of 0 0036 ft/ft across the <br /> site Specific conductance ranged from 850 to 1,100 µS. <br /> Total BTEX concentrations ranged from 5000 to 24,000 ppb in <br /> groundwater samples The vertical extent of hydrocarbon contamination extended <br /> to a maximum depth of 15 ft (4 6 m) sub-grade. No light non-aqueous phase <br /> liquid (LNAPL) was observed at the site Dissolved oxygen contents in the <br /> groundwater were below 1 ppm in nearby monitoring wells. <br /> Combined air/ozone flow to the recirculation well was 2.2 cfm. The <br /> system was set to run 18 minutes for the lower Spargepoint®, 11 minutes for the <br /> in-well Spargepoint®, and 5 minutes for the submersible pump. The system <br /> operated on 14 cycles of 34 minutes each during a 24-hour period. <br /> Monitoring was performed during a 20-day test period on the site, <br /> beginning July 29, 1997. Analytical results from a monitoring well located 18 ft <br /> (5 5 m)from the main recirculation well (CS-i) are presented in Figure 3. During <br /> the period of the 20-day test, total BTEX plus MTBE concentrations dropped <br /> from 19,220 ppb to 1004 ppb This represents a reduction of 94 80/a during the <br /> test penod. MTBE concentrations dropped from 520 ppb to 6 ppb during the test <br /> period,representing in excess of 99% removal during ozone treatment. <br /> Site 2: Upgradient of Water Supply Well. An oxidative curtain, or "bubble <br /> fence", was employed to attempt to contain an advancing MTBE plume <br /> threatening a water supply well near Lake Tahoe, California. The soil consisted <br /> of silty, clayey sand The static groundwater level at the time of installation was 5 <br /> ft (1 5 m) below grade, although levels are known to drop to 10 ft (3 m) below <br /> grade A groundwater gradient of 5 ft (1 5 m) per 40 ft (12.2 m), or 0 125 ft/ft, <br /> was measured. The observed forward advance of the plume was between 3 ft <br /> (1 m) to 10 ft (3 m) per month The bottom of the contaminated zone was 20 ft <br /> b <br />