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ARCHIVED REPORTS_XR0005324
Environmental Health - Public
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3500 - Local Oversight Program
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PR0545550
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ARCHIVED REPORTS_XR0005324
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Last modified
3/16/2020 8:13:30 PM
Creation date
3/16/2020 4:51:17 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
3500 - Local Oversight Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0005324
RECORD_ID
PR0545550
PE
3528
FACILITY_ID
FA0003973
FACILITY_NAME
SHOCKEY & SONS TRUCKING
STREET_NUMBER
850
STREET_NAME
MILGEO
STREET_TYPE
RD
City
RIPON
Zip
95366
CURRENT_STATUS
02
SITE_LOCATION
850 MILGEO RD
P_LOCATION
05
P_DISTRICT
005
QC Status
Approved
Scanner
SJGOV\sballwahn
Tags
EHD - Public
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1 � <br /> ' 20 December 2002 <br /> AGE-NC Project No 95-0185 <br /> ' Page 5 of 7 <br /> ' The remaining annular space was filled to within one and one-half foot of the ground surface with <br /> a cement grout The grout mixture consisted of type VII portland neat cement and not more than six <br /> gallons of water per 94-pound sack of cement As-built ozone-sparge point/monitoring well- <br /> construction diagrams are included in Appendix C <br /> ' 2 3 5 Equipment Decontamination <br /> The hollow stem augers were steam cleaned prior to each bore-hole advancement Sampling tools <br /> ' and brass sleeves used for sample collection were thoroughly washed with a solution of Alconox, <br /> and were thoroughly rinsed with clean tap water prior to each sampling run Following drilling <br /> activities, nnseate generated from decontaminating the equipment was placed in properly labeled <br /> ' DOT-approved model 17H 55-gallon drums and was stored on-site In an area lacking public access <br /> ' 2 3 6 Well Elevation Survey <br /> On 22 November 2002, a California state-licensed survey engineer from Baumbach&Piazza,Inc <br />' surveyed a reference point on the casing tops of the monitoring wells to the nearest 0 01-foot relative <br /> to San Joaquin County Bench Mark Datum BM # LM-38 6 The results of the monitoring well <br />' survey are contained in Table 1 The surveying report (Baumbach & Piazza Job No 9797) is <br /> presented in Appendix D <br /> 1 3.0. FINDINGS <br />' The stratigraphy and ground water elevation, gradient and flow direction were determined from the <br /> field data Contaminant impact to soil and ground water were assessed by laboratory analysis <br />' 31 STRATIGRAPHY <br />' The soil consisted predominantly of tan-brown silt from a depth of approximately 5 feet to 20 feet <br /> bsg Tan silty sand was encountered at depths of 5 and 25 feet bsg, and poorly graded saturated sand <br /> was encountered at the total depth of soil boring MW-5 (30 feet bsg) Soil boring logs and well <br /> construction diagrams are depicted in Appendix C <br /> 1 <br />' Advanced GeoEnVLronmental,Inc <br />
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