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i <br /> were relatively low (18 6 parts per million by volume on August 16, 2005), this well was disconnected and <br /> well MW-4 was connected for soil vapor extraction on August 22, 2005 <br /> Operation and Maintenance <br /> During first quarter 2006, Stratus conducted twelve site visits to verify the system operation, to optimize <br /> system performance, conduct routine maintenance, and to collect the required discharge samples <br /> Currently the SVE system is set-up to extract soil vapors from wells VW-1, VW-3, VW-4, VW-8, VW-14, <br /> MW-4, MW-8, and MW-9 The SVE system was observed to be non-operational on January 24, 2006, <br /> due to low propane The system was re-started on the same day after a propane re-fill The SVE system <br /> was observed to be non-operational on February 14, 2006, due to the air pressure alarm Based on the <br /> hour meter readings for January 27 and February 14, 2006, the SVE system was likely shutdown on <br /> January 28, 2006 The SVE system was re-started on February 14, 2006, by adjusting the influent air flow <br /> rate The SVE system was again found to be non-operational on March 21, 2006, due to low propane <br /> Based on the hour meter readings for March 15 and 21, 2006, the SVE system was likely shutdown on <br /> March 20, 2006 The SVE system was re-started on March 23, 2006, after re-filling the propane tank <br /> During the first quarter 2006 (between December 21, 2005 and March 28, 2006), the SVE system <br /> operated for 1,884 9 hours with an average operational uptime efficiency of 82 percent The GRO and <br /> benzene concentrations in the influent air samples collected during first quarter 2006 were in the range of <br /> 6,000 to 15,000 Mg/M3 and 34 to 210 mg/m3, respectively The average system Influent airflow rate to the <br /> SVE system was observed at 292 67 cfm at an average applied vacuum of 100 49 inches of water <br /> column During the first quarter 2006 (between December 7, 2005 and March 1, 2006), approximately <br /> 37,843 82 pounds of GRO were extracted and abated by the SVE system A cumulative mass of <br /> approximately 77,507 47 lbs (Figure 6) of GRO has been removed from the subsurface by both the two <br /> 200 cfm (previously operated) and the current 500 cfm SVE systems The SVE system is operating as <br /> designed and is in compliance with the SJVPACD permit requirements <br /> ATTACHMENTS <br /> • Table 1 Product Monitoring and Removal Summary <br /> • Table 2 Groundwater Level Data <br /> • Table 3 Groundwater Analytical Summary <br /> • Table 4 Groundwater Analytical Results for Oxygenates and Additional Compounds <br /> • Table 5 Summary of Wells <br /> • Table 6 Flow Rates and Analytical Results of Air Sample Analyses <br /> • Table 7 Operational Uptime and Flow Rate for SVE System <br /> • Table 8 Extraction and Emission Rates <br /> • Figure 1 Site Location Map <br /> • Figure 2 Site Plan <br /> • Figure 3 Groundwater Elevation Contour Map, Upper Water Bearing Zone (1st Quarter 2006) <br /> Figure 4 Groundwater Elevation Contour Map, Lower Water Bearing Zone (1st Quarter 2006) <br /> Figure 5 Groundwater Analytical Summary(First Quarter 2006) <br /> • Figure 6 Influent GRO Concentrations in Soil Vapors and Cumulative GRO Mass Removed <br /> Over Time <br /> • Appendix A Field Data Sheets <br /> • Appendix B Sampling and Analysis Procedures <br /> • Appendix C Certified Analytical Reports with Chain-of-Custody Documentation and EDF <br /> Verification <br /> • Appendix D Performance and Operation Summary of King, Buck, & Associates SVE Systems <br /> K 1Bp-Arco for URS161001Quarterly120061Arco 6100_1 Q06 doc STRATUS <br />