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i <br /> Appendix A - Historical Background <br /> PACIFIC MINI-MART <br /> 4511 Pacific Avenue, Stockton, California <br />' was calculated at 205 ft'/day(equivalent to 1,536 gallons per day/ft) and a storativity value <br /> was calculated at 0 054 <br /> • Based on a transmissivity value of 205 ftz/day and the extraction well screen thickness equal <br />' to 25 ft (screen Interval at EW-1), a hydraulic conductivity value was calculated at <br /> 6144 ft/day, or 0 022 cm/s, a hydraulic conductivity of 0 022 cm/s is consistent with a <br /> screened Interval located within a well sorted sand to clean sand <br /> I0 Laboratory analysis of extracted water during the pumping test detected elevated <br /> concentrations of TPH-g, BTEX and MTBE <br /> On 05 and 06 June 2001 four ground water monitoring wells were Installed off-site as part of the <br /> Investigation Borings MW13 through MW16 were completed as ground water monitoring wells <br /> MW-13 through MW-16 MTBE was detected in the soil samples collected from thirty feet bsg from <br /> borings MW 15 and MW 16, these concentrations maybe more reflective of impacted groundwater <br /> in the pore spaces of the soil than of adsorbed MTBE <br /> The highest concentration of dissolved hydrocarbons quantified as TPH-g,TPH-d and overall BTEX <br /> • compounds occurs in the areas east and northeast of the dispenser Islands, on-site The highest <br /> concentration of MTBE detected in the ground water occurs in monitoring well MW-11, which is <br /> situated in the median of Pacific Avenue Lower or non-detectable concentrations in the down- <br /> gradient and cross gradient wells define the dissolved MTBE plume toward the north and west This <br /> suggests that the dissolved MTBE plume is detaching from the TPHBTEX hydrocarbon plume <br />' <br /> In September and October 2001, a low-flow, ground water extraction and treatment system was <br /> Installed at the site The system utilizes the newly installed ground water extraction well on site and <br /> a small volume treatment system As of 16 December 2002, approximately 1,315,454 gallons of <br />' hydrocarbon-Impacted ground water have been extracted and treated for disposal <br /> On 04 and 05 February 2003 two additional ground water monitoring wells were installed oft-site <br />' as part of the Investigation Boring MW 17 was completed as groundwater monitoring well MW-17 <br /> using two-Inch diameter PVC casing with 0 020-Inch slotted screen installed from approximately <br /> 25 feet to 45 feet bsg and boring MW18 was completed as ground water monitoring well MW-18 <br /> o,"ev tx,r�_Infh diameter 1P-x7(— oagirnv with n 4 O-inr-h clnttarl ,rrFPn installed f om approximately <br /> �b a <br /> 60 feet to 65 feet bsg and with blank casing extended to the surface <br />' At that time,the dissolved MTBE plume has been defined down-gradient of the site(east)by wells <br /> MW-12, MW-16, MW-17 and 18 <br /> Advanced GeoEnvironmental Inc <br /> I <br />