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ARCHIVED REPORTS_XR0012886
Environmental Health - Public
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2900 - Site Mitigation Program
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PR0528359
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ARCHIVED REPORTS_XR0012886
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Last modified
5/8/2020 3:36:06 PM
Creation date
5/8/2020 3:20:46 PM
Metadata
Fields
Template:
EHD - Public
ProgramCode
2900 - Site Mitigation Program
File Section
ARCHIVED REPORTS
FileName_PostFix
XR0012886
RECORD_ID
PR0528359
PE
2950
FACILITY_ID
FA0019146
FACILITY_NAME
SHELL OIL PRODUCTS US
STREET_NUMBER
3725
Direction
N
STREET_NAME
TRACY
STREET_TYPE
BLVD
City
TRACY
Zip
95304
APN
21217030
CURRENT_STATUS
02
SITE_LOCATION
3725 N TRACY BLVD
P_LOCATION
03
P_DISTRICT
005
QC Status
Approved
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EHD - Public
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Aug 12 02 08 : 04a : p. 2 <br /> Water Well Technology, Inc. Y <br /> License No.C57-731133 - <br /> a P.O. Box 519 Fair Oaks,Ca 95628 <br /> (800)961-WELL (916)961-9355 Fax (916) 961-1773 <br /> August 7, 2002 VISUAL WELL LOG <br /> Cambria Environmental <br /> Well Shell 3725 Tracy Boulevard <br /> o Casino steel 6 in. <br /> 7' Static kN21er'e al;clear) <br /> 4eavyincrustatio., REASON FOR VIDEO: <br /> 2v - <br /> Check condition for abandonment <br /> Deterioration and holes <br /> j AREA VIEWED: <br /> r Ground to 115 ft. { <br /> 40 EVALUATION FROM SURVEY: j <br /> < d. Casing: Poor condition/thin and deteriorated!heavy incrustation. <br /> I <br /> Perforations:Vertical slots/ few visible due to encrustation. <br /> y <br /> Total depth: 115 ft. <br /> 60 —4— <br /> AREAS <br /> AREAS OF CONCERN: 1 <br /> _7 1)Ofd cable toot well,likely does not have a proper surface seal. <br /> 1; =- - 2)Plugged perforation. <br /> i 80 3)Deterioration due to age of casing. <br /> i <br /> ` r NOTES & SUGGESTIONS: <br /> Due to condition of casing it would be better to blast perforate with 3 <br /> 100 +>> sealing material in the well rather then mechanical perforate and have <br /> caving or stuck toots. <br /> 107'to 135' Perforations <br /> 115'8c;ton <br /> 120 Drilled depth un:mcwn <br /> i <br /> i <br /> SURVEY BY:Renee <br /> EVALUATION BY:Robert J.Guardino <br /> 11 you have any questions regarding this report } <br /> please call 915 961.9355 <br /> i <br /> r <br /> r <br /> The accuracy of this report is based on the video survey and information given to WWTI.The comments and <br /> recommendations are the opinions of 1VWT1 based on this information.Other information not known to WWTI <br /> may change the opinions expressed in this report. 1 <br /> L <br />
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