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x.00' <br /> ASS(VYATC <br /> o C I ATE S INC'. <br /> test was approximately 1.5 hours in length. Flowrates, applied vacuums, influent and effluent <br /> volatile organic compound (VOC) concentrations, and temperatures were also monitored_during <br /> the test; Vapors were extracted using an internal combustion (IC) engine equipped with:a 5-hp <br /> blower and a moisture knockout chamber. Two influent vapor samples and one effluent vapor <br /> sample were collected during the test. Results and field readings from the short-term vapor <br /> extraction are summarized in Tables 4 and 6. <br /> During the vapor extraction test, extraction flowrates ranging from 47 to 57 cubic feet per minute <br /> (cf n)resulted in vacuums of up to 0.8 inches of water in vadose wells VW-5s and VW-2d located <br /> 17 feet from the extraction well. No response was observed in wells MW-1 and VW4, located <br /> just 6 to 7 feet from the extraction well. This may have been due to preferential pathways present, <br /> in the subsurface or because the wells are screened approximately 8 to 13 feet below the current <br /> water table. Vacuums of up to 0.5 inches of water were observed in well MW-3 located 87 feet <br /> away which is screened approximately 3 feet below the water table. Laboratory results of the <br /> vapor samples indicated that volatile hydrocarbons were detected in the influent samples. <br /> Approximately 0.2 pounds of total petroleum hydrocarbons as gasoline (TPHg) was removed <br /> during the pilot test. Laboratory results of the effluent vapor sample indicated a destruction <br /> efficiency of approximately 70 percent for benzene and over 98 percent for all other constituents <br /> analyzed. <br /> On November 24, 1998, a short-term air sparge test was initiated by ATC using vapor well VW- <br /> 5d as the air injection point, Upon startup of the test, an'air leak was observed in nearby vapor <br /> well VW-2s from an apparent crack in the well seat, The test was terminated and provisions were <br /> made to abandon well VW-2s. <br /> On February 17, 1999, ATC supervised the abandonment of vapor well VW-2s. It was proposed <br /> in the workplan to pressure grout the well with neat cement from the bottom of the casing to the <br /> surface using a trernie pipe but an unknown obstruction was encountered at 9 feet-bsg and it was <br /> not passible to lower the tremie pipe past this depth. A direct push drill rig was used to attempt <br /> W:\62574.01\CAP report doa 5 <br />