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Treadwell&Rollo <br /> Soil sampling conducted around the former UST location has identified high TPHg <br /> concentrations in soil above the water table These TPHg results range from 8,100 milligram per <br /> kilogram (mg/kg) in boring 16B-8 (Treadwell & Rollo, 2004) up to 14,000 mg/kg in VW5 <br /> (AGE, 1999) at a depth of 10 to 11 feet bgs These results indicate that a continuing source of <br /> contamination was present in this area Previous soil sampling results also indicate that high <br /> TPHg concentrations (9,000 mg/kg in VW5 at 25 feet bgs and 8,300 mg/kg in SW21 at 35 feet <br /> bgs) exist below the current groundwater table in this area (AGE, 1999) This is likely residual <br /> contamination from when the groundwater table was deeper than 25 feet bgs <br /> As previously reported in the 2004 Workplan, boring logs indicate that separate phase product <br /> may be present in soil and groundwater within the former UST location extending to at least <br /> 16B-8 to the west and MW-3 to the east Significant,but lower TPHg concentrations are present <br /> in soil (at the groundwater interface) and/or in groundwater in borings 16B-10 to the south, and <br /> in boring 16B-713 and well EW-4 to the north TPHg and benzene concentrations in groundwater <br /> drop off beyond this area in borings 16B-9 and 1613-11, and appear to be related to the "smear <br /> zone" or the depth interval of groundwater table fluctuation <br /> This data suggested that there has been a continuing source of gasoline contamination at the <br /> former Tank No 7 location, and that free product may have been present This would account for <br /> why years of in-situ remediation work has not resulted in more significant decreases in <br /> groundwater concentrations at the Tank No 7 location, and may indicate that continued in-situ <br /> remediation may not effectively mitigate the groundwater contamination <br /> 4.0 SITE REMEDIATION <br /> The Site excavation activities are described in Sections 4 1 to 4 7 Deviations from the 2004 <br /> Workplan are presented 1n Section 4 2 <br /> 25971021 DJS 4 18 November 2004 <br />