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Table 2. Groundwater Chemical Data <br /> Well# Date TPHG Benzene Toluene Etb lbenzene Xvlene MTBE <br /> u <br /> MW-1 12/05/94* 48,000 2100 510 1900 3000 NA <br /> MW-1 04/03/95 82,000 380 150 310 620 NA <br /> MW-1 06/16/95 46,000 160 130 110 200 NA <br /> MW-1 09/14/95 28,000 240 31 130 160 NA <br /> MW-1 12/26/95 35,800 8000 2100 9000 1800 NA <br /> MW-1 03/28/96 34,000 51 20 34 50 NA <br /> MW-1 06/27/96 28,000 110 39 80 130 NA <br /> MW-1 09/23/96 36,000 110 39 73 97 NA <br /> MW-1 12/19/96 60,000 180 81 110 150 NA <br /> MW-1 03/10/97 16,000 86 17 37 49 NA <br /> MW-1 06/30/97 38,000 110 20 82 100 NA <br /> MW-1 08/20/97 13,000 17 43 22 27 NA <br /> MW-1 12/10/97 No rept 530 55 350 440 NA <br /> MW-1 03/31/98 9,000 1400 130 880 500 NA <br /> MW-106/30/98 9,100 860 150 1000 940 NA <br /> MW-1 09/29/98 8,400 960 92 860 580 NA <br /> MW-1 12/29/98 9,100 910 150 990 840 NA <br /> MW-1 03/29/99 13,000 790 140 1000 900 NA <br /> MW-1 Monttormg well destroyed June 1999 during source removal cleanup <br /> MW-2 12105194* <200 ND ND ND ND NA <br /> MW-2 04/03/95 ND ND ND ND ND NA <br /> . MW-2 06/16/95 ND ND ND ND ND NA <br /> MW-2 09/14/95 ND ND ND ND ND NA <br /> MW-2 12/26/95 ND ND ND ND ND NA <br /> MW-2 03/28/96 ND ND ND ND ND NA <br /> MW-2 06/27/96 ND ND ND ND ND NA <br /> MW-2 09/23/96 ND ND ND ND ND NA <br /> MW-2 12/19/96 ND ND ND ND ND ND <br /> MW-2 03/10/97 ND ND NO ND ND ND <br /> MW-2 06/30/97 ND ND ND ND ND ND <br /> MW-2 08/20/97 ND ND ND ND ND ND <br /> MW-2 12/10/97 ND ND ND ND ND 59 <br /> MW-2 03/31/98 ND ND ND ND ND ND <br /> MW-2 06/30/98 ND ND ND ND ND ND <br /> MW-2 09/29/98 ND ND ND ND ND ND <br /> MW-2 12/29/98 ND ND ND ND ND ND <br /> MW-2 03/29/99 ND ND ND ND ND ND <br /> MW-2^ 06/30/99 ND ND ND ND ND ND <br /> MW-2^ 10/05/99 ND ND ND ND ND ND <br /> MW-2 01/27/00 ND ND ND ND ND ND <br /> MW-2 04/20/00 ND ND ND ND ND ND <br /> MW-2 07/19/00 ND ND ND ND ND ND <br /> ND-None detected NA-Not Analyzed ug/I-micrograms per Mer <br /> *-Samples not analyzed at RWQCB detection limits for this sampling event <br /> MTBE-Methyl-Teri-Butyl-lather and fuel oxygenates by Method 8260 from 3/3/98 forward <br /> no rept -laboratory had insufficient quantity to quantify TPHG <br /> ^-Very low VOC detected June 1999 1 2-Dtchloroethane was ND for all wells for 3/19/99 sampling <br /> Laboratory reports that this did not match their gasoline standard <br /> M&M Automotive Quarterly Monrtonng Report Page 4 <br /> Wnght Environmental Services, Inc <br /> 8/18%2000 <br />