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Fourth Quarter 2004 <br /> Thrifty#171 <br /> January 18, 2005 <br /> Page 2 <br /> A summary of historical analytical sampling results for TPHg,BTEX, and MTBE is provided in <br /> Table 1, and oxygenate/alcohol results are summarized in Table 2 Copies of the EMC Field <br /> Status Reports are presented in Appendix A, and copies of the laboratory analytical reports are <br /> contained in Appendix B <br /> TPHg, benzene, and MTBE isoconcentration maps are presented as Figures 2, 3, and 4, <br /> respectively The analytical laboratory results indicate that the highest groundwater <br /> concentrations of TPHg, benzene, and MTBE were found in monitoring well MW-5 (149,000 <br /> ug/L, 15,200 ug/L, and 19,900 ug/L, respectively) D1PE, ETBE, TAME, and TBA were not <br /> detected with the exception of TBA in wells MW-2 (253 ug/L), MW-3 (58 ug/L), MW-5 (2,220 <br /> ug/L), MW-6 (258 ug/L), T13-8 (56 ug/L), TB-9 (54 ug/L), and TB-12 (6,400 ug/L) Ethanol and <br /> methanol were not detected above 20 milligrams per liter A trace concentration of 4 3 ug/L 1,2- <br /> DCA was detected in well TB-10, but was not detected in the other wells <br /> Remediation Status <br /> iOn July 1, 1999, a Balser Furnace Thermal Oxidizer Unit was placed into operation, to destroy <br /> vapors extracted by the SVE system Presently, the remediation system is connected to SVE <br /> wells MW-2, MW-4, MW-5, T13-3, T13-4, TB-6, TB-7, T13-9 (A, B), TB-11 (A, B), and TB-12 <br /> (A, B) A map presenting the extraction well layout is shown as Figure 5 The only wells <br /> operating this quarter were TB-11 wtr (50%), MW-5 (100%), and TB-3 (50%) <br /> During this reporting period, the soil vapor extraction unit operated approximately 967 hours and <br /> approximately 1,169 pounds of hydrocarbon as TPHg were removed this quarter as of December <br /> 27, 2004 (Table 3) The cumulative system total as of December 27, 2004, was approximately <br /> 31,138 hours of operation and approximately 141,751 pounds of hydrocarbon as TPHg removed <br /> The system operated throughout the quarter except when it was shut down for quarterly water <br /> sampling from November 22 though November 29, 2004 The system was also found to be <br /> down on October 11, October 18, October 25, November 8, November 22, December 13, <br /> December 20, and December 27, due to mechanical problems In each case, the system was <br /> restarted the same day Field records of the SVE system are provided in Appendix C <br /> Vapor samples were collected from the system inlet and outlet ports on October 11, 2004, <br /> November 8, 2004, and December 6, 2004 Vapor samples from selected wells were collected on <br /> November 8, 2004 The samples were analyzed for TPHg by EPA Method 8015M for gasoline, <br /> BTEX, and MTBE by EPA Method 8021B <br />