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rg NFID INTIAL' <br /> U <br /> Section 3 <br /> Observation of a Lining' Installation in Oklahoma <br /> MRI had the opportunity to observe an actual lining installation during the period <br /> from May 31 through June 2, 1995. The purpose of our observations was to compare <br /> the installation operation with the recommendations in API 1631. <br /> The lining operation was performed at a Phillip's Gas & Go at 528 S. Chickasaw in <br /> Pauls Valley, Oklahoma, south of Oklahoma City. The facility was a fairly large <br /> operation, with six pumps, a convenience store, a drive-up snack window, and a car <br /> wash. More than one tank was to be lined; we observed all but the initial steps on one <br /> tank and the beginning of the process on a second tank. The first tank was a nominal <br /> 10,000-gallon steel tank 96 inches in diameter and 27 feet long. <br /> The firm doing the work, as licensed by IECC, was Rockey's, Inc., from Topeka, <br /> Kansas. When we arrived on the job site the morning of May 31, a crew based in <br /> Topeka had already broken concrete, removed product, cut a manway, and de-sludged <br /> the tank The following paragraphs present our observations relative to API 1631. <br /> A general site inspection showed that there were no ignition sources present, the <br /> area was properly cordoned off, appropriate fire extinguishes were present, and that <br /> proper safety procedures were being carried out. Figure 1 shows a general view of the <br /> site. All equipment appeared to be properly grounded. The crew members wore proper <br /> safety gear, depending on the phase of the operation. The, foreman reported that all had <br /> been through the proper training courses. <br /> An MSA (Mine Safety Appliances) combustible gas indicator had been used to <br /> assure that the area was free of hazardous vapors. We inspected the device and found it <br /> to be in apparently good operating condition. The foreman said that it is calibrated by a <br /> laboratory semiannually. The initial ventilation was performed using a diffused air <br /> blower (method 2.4.3.2 of API 1631), which we checked OUL After the tank was <br /> deemed free of harmful vapors, continuous ventilation was provided by a squirrel cage <br /> blower (see Figure 2). This blower had an explosion-proof motor and supplied air to <br /> the tank through a 12-in flexible hose. <br /> The manway was cut to the 18-in x 18-in size required by API 1631. The <br /> sludgetabsorbent mix that was removed from the tank was placed into steel drums, <br /> which were sealed and turned over to the station operator for proper disposal. Some of <br /> these drums may be seen in Figures I and 2. Although the sludge was not tested for <br /> the presence of lead compounds, the crew followed their normal practice of handling <br /> the material as if it did contain lead, benzene, or other hazardous materials. <br /> &M-Apptkd,R4M9.FR 4 <br />