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r <br /> r NINIIAL <br /> Section 4 <br /> Supplemental Observations <br /> To supplement the information presented in the previous section, the author had the <br /> opportunity to observe another lining installation operation with the IECC product in <br /> Colorado. In addition, a full report of an interior ultrasonic integrity inspection <br /> conducted in California was obtained and reviewed. Each of these is discussed here. <br /> 4.1 Colorado Tank Lining Observations <br /> On July 19 and 20, 1995, the author had the opportunity of observing a tank lining <br /> operation with the IECC EC 125.lining material in the Denver, Colorado area. <br /> Specifically, the observations occurred at a Bradley Self-Serve station at 3485 West <br /> 72nd Street in Westminster, Colorado, a suburb north of Denver. The station has six <br /> underground tanks, three of which were to be lined and three were to be taken out of <br /> service and removed. The lining work was being performed by Rockey's, Inc., but by a <br /> crew out of Colorado Springs, not Topeka. We had the opportunity during the course <br /> of four visits to the site (while conducting other business in the Denver area) to observe <br /> almost all facets of the operation. To avoid repetition, only our observations that <br /> supplement those.in Section 3 will be given here. <br /> After pumping out a tank, purging was begun using method 2.4.3.2 of API 1631. <br /> A brass air-diffusing pipe was inserted into the fill opening, resting on the tank bottom <br /> and grounded to the opening. The pipe had four rows of small holes running its length <br /> for introducing air into the tank. Compressed air was delivered to the pipe through a <br /> fitting with a pressure regulating valve and gauge, to maintain no more than 5 psi of <br /> pressure. Figure 4 shows the diffused-air blower setup. Vapors were vented from the <br /> tank's vent pipe. <br /> An MSA combustible gas indicator was used to monitor the gas being vented. <br /> When the reading dropped below 20% of the lower flammable limit (LFL), purging was <br /> continued and a small hole was drilled into the tank using an air-driven drill and <br /> lubricating oil. Then a long probe was inserted into the hole and monitoring of the <br /> atmosphere inside the tank was conducted, as purging was still being continued. This is <br /> shown in Figure 5. Finally, after the reading dropped below 10% of the LFL, three <br /> more holes were drilled in the tank to outline the comers of the manway opening. <br /> Then, while continuing to purge, an air-driven power saw was used, with copious <br /> amounts of lubricating oil, to cut between the holes. As the last cut was being <br /> completed, another crew member supported the cut plate and lifted it out. <br /> MRI-APPSOM4069-PR 8 <br />