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Chevron 0 <br /> w. ing <br /> 55 31� <br /> Gur Fame lB1.1d, <br /> Chevron Corporation <br /> 145 S. State College <br /> Brea, CA 92821 <br /> April 11,2016 P.O. Box 2292 <br /> Brea, CA 92821-2922 <br /> San Joaquin County <br /> Environmental Health Departmente�•�o(wF�����® <br /> 1868 East Hazelton Ave. <br /> Stockton,CA 95205 <br /> JUN 2 3 2016 <br /> ENV1RONIPAENTAI H <br /> Inspector Vicki McCartney, <br /> PERMIT/SERVIOES�TH <br /> This letter is in response to the inspection report issued on Feb 10&Mar 4,2016 to Chevron Station#208117 located at 755 S Tracy Blvd. <br /> Tracy,CA. <br /> Below is our response regarding the 4 items noted in the enclosed inspection report; <br /> • Designated operator employee training not performed or log not kept.Designated operator failed to list the hire date for one <br /> employee on the training log. <br /> o Per the enclosed inspection report,the log was corrected on site. <br /> • Primary containment not tight.Weeping at the sheer valve and above the sheer valve was observed in disp 3/4 and 7/8,indicating a <br /> leak in the primary pipping. <br /> o Per the enclosed inspection report,the service technician removed the product from the pipes and this appeared to have <br /> corrected the weeping of product.Corrected on site. <br /> • The supreme 91 and regular 87 product line leak detector failed to detect a simulated leak when tested. <br /> o Per the enclosed inspection report,the technician replaced the siphon jet on the 87 LLD and the subsequent testing <br /> passed.Corrected on site. <br /> o Per the enclosed inspection report dated 03/04/2016;on Feb 10,2016 Service Station System Inc arrived at the site and <br /> replaced the 91 product STP check valve and performed the 3GPH leak test at 10 pounds per square inch(PSI)pressure <br /> and test passed.On Mar 4,2016 the 91 LLD and the"sensor out"'fail safe"on disp 11/12 was retested by Tanknology <br /> and testing passed. <br /> • The 87 product STP sump boot was clamped shut and the schreider valve was pointed up. <br /> o The Tanknology service technician was able to remove the boot and point the schreider valve down.Corrected on site. <br /> ASin <br /> 4,il(consie above items resolved per this letter.Please contact me directly if you have any questions or concerns. <br /> Compliance Coordinator <br /> Chevron Stations Inc. <br /> 145 S.State College.,Suite 400 <br /> Brea,CA 92821 <br /> Office Phone(714)6713223 <br /> Cell Phone(909)420 5289 <br /> Fax(866)420 0335 <br /> (Please use fax cover) <br /> Mailto:MohsinKhwaia@Chevron.com <br /> Enclosed Documents:Copy of inspection report dated 02/10/2016 and 03/04/2016. <br />