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17ECTOR <br /> ENGINEERING INC. <br /> 0 ®ALLY CONSTRUCTION FIELD REPORT <br /> Project Name: Project No. Daily Field Report Sequence Number: <br /> Forward Landfill 021605.03 34 <br /> Location of Work: Client Or Manager Date: Day of The Week: <br /> Manteca,Ca Butch Stefan Forward, Inc. October 15,2003 1 Wednesday <br /> General Contractor: Liner Contractor: Project Engineer: <br /> Sukut Construction GSE <br /> General Foreman: Liner Superintendent: Other: <br /> Jim Hasal Air King Bailey Sukut <br /> Source and Description of Fill Material: Weather: CQA Technician: <br /> On site native, light brown silty CLAY Warm, clear and Ken Davila <br /> breezy <br /> Equipment on site: <br /> 1-D6 dozer, 1-water truc 1-D5 dozer,2-633 sora ers, 1- 16G blade, 1-825 com actor <br /> NOTES(Describe work completed during the day,any problems and their solutions): <br /> I arrived on site and met with the Sukut foreman to discuss the testing and sampling locations at the <br /> location listed above. The 16G blade cut the north and west FU-03 cell floor areas through the day's shift. <br /> The D6 dozer and the D5 dozer cut the west and south slopes FU-03 cell as one scraper hauled the excess <br /> cut material to the fill area on the floor. The other scraper continued hauling clay out of the stockpile to the <br /> east and placing it on the north central floor. The 825 sheepsfoot supplied compactive effort to the native <br /> clay throughout the day. <br /> In the early morning, two(2)trucks arrived on site with a total of thirty-two rolls of geosynthetic clay <br /> liner(GCL). The material was logged in, checked for damage, and unloaded. GSE personnel unloaded the <br /> trucks and filled sand bags for the rest of the day. <br /> Three(3)drive tube permeability samples were obtained and were taken to off site Vector personnel for <br /> delivery to the laboratory this evening. Five(5)nuclear moisture density tests were performed at random <br /> locations and elevations on the native clay in the FU-03 cell. All tests passed the 90 percent compaction <br /> specification and also passed the moisture content specification. The on site foreman was verbally informed <br /> of the test results. <br /> In the early afternoon,an on site weekly meeting was held to discuss project progress and scheduling. The <br /> current schedule projects a completion date of approximately January 7 ,2004. <br /> On site lab testing of the clay material continued with two(2) sieve analysis samples washed and placed <br /> into the oven for tomorrow's testing. <br /> Prepared By: Reviewed By: <br /> 4/23/03,Rev. 0 1 of 1 <br /> r-? <br />