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S ■ J O A Q■.I N Environmental Health Department <br /> COUNTY <br /> Underground Storage Tank Program Inspection Report <br /> Facility Name: Facility Address: Date: <br /> Colonial Energy CE 40134(DBA Power Mart) 1434 W Yosemite Ave, Manteca JOctober 04, 2018 <br /> Item# Remarks <br /> 211 CCR 2715(c)(2) No employee present that were trained in the operation and maintenance of the UST system by a <br /> DO. <br /> The designated operator employee training for Danielle Hook, Brian Jordan, Isaiah Garcia, Schelby Horton, and Jeff <br /> Atteberry did not have the hire date of the employees. The designated operator shall train facility employees for <br /> which he or she is responsible in the proper operation and maintenance of the UST system once every 12 months. <br /> The training shall include, but is not limited to: <br /> 1. Operation of the UST system in a manner consistent with the facility's best management practices <br /> 2. Employee's role with regard to monitoring equipment as specified in the facility's monitoring plan <br /> 3. Employee's role with regard to spills and overfills as specified in the facility's response plan <br /> 4. Name of the contact person(s)for emergencies and monitoring equipment alarms <br /> Ensure that employees have been trained by the designated operator, maintain the list on site, and submit a copy of <br /> the training records to the EHD. The manager on site was able to add the missing dates to correct this violation on <br /> site. <br /> This was corrected on site. <br /> This is a minor violation. <br /> 315 HSC 25291(e)Water in secondary containment not removed, analyzed, and properly disposed of(pre-Jul 2003). <br /> Liquid was observed in the 87 product STP, Diesel STP, UDC 7/8,and UDC 5/6 sump. If water could enter into the <br /> secondary containment by precipitation or infiltration, it must be removed and disposed of properly. The service <br /> technician removed the liquid from the 87 product STP, Diesel STP, UDC 7/8,and UDC 5/6 sump. Ensure that all <br /> sumps and annular spaces are maintained free of liquid. <br /> This was corrected on site. <br /> This is a repeat violation, Class II. <br /> 318 CCR 2636(f)(2) Leak detector failed to detect a 3.0 gallons per hour leak at 10 pounds per square inch. <br /> The 91 product VMI line leak detector failed to detect a leak when tested. All line leak detectors shall be capable of <br /> detecting a 3-gallon per hour leak at 10 psi. The service technician adjusted the leak detector, retested it, and it <br /> passed. <br /> The Diesel product line leak detector failed to detect a leak when tested. All line leak detectors shall be capable of <br /> detecting a 3-gallon per hour leak at 10 psi. Immediately have a properly licensed,trained, and certified contractor <br /> repair or replace the failed leak detector(LG 113-x listed, if applicable)and obtain a permit within one business day <br /> from the EHD. If the failed leak detector can't be replaced immediately, there is a possibility that the Diesel product <br /> UST system may be red tagged to prevent fuel inputs. <br /> This is a minor violation. <br /> Overall Inspection Comments: <br /> Complete and submit a copy of the Return to Compliance Certification form to the EHD with a statement <br /> documenting the corrective actions that have been or will be taken for each violation, and any supporting <br /> paperwork, by November 3rd, 2018. <br /> FA0003739 PR0231465 SCO01 10/04/2018 <br /> EHD 23-01 Rev.09/28/2018 Page 4 of 5 Underground Storage Tank Program OIR <br /> 1868 E. Hazelton Avenue I Stockton, California 95205 1 T 209 468-3420 1 F 209 464-0138 1 www.sjcehd.com <br />