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ARCHIVED REPORTS_MONIT RPTS
Environmental Health - Public
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EHD Program Facility Records by Street Name
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A
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AIRPORT
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401
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4200 – Liquid Waste Program
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PR0526172
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ARCHIVED REPORTS_MONIT RPTS
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Last modified
12/3/2020 7:43:29 PM
Creation date
8/5/2020 10:00:32 AM
Metadata
Fields
Template:
EHD - Public
ProgramCode
4200 – Liquid Waste Program
File Section
ARCHIVED REPORTS
FileName_PostFix
MONIT RPTS
RECORD_ID
PR0526172
PE
4242
FACILITY_ID
FA0017710
FACILITY_NAME
ANKA NORTHSTAR
STREET_NUMBER
401
Direction
S
STREET_NAME
AIRPORT
STREET_TYPE
WAY
City
MANTECA
Zip
95336
APN
24130052
CURRENT_STATUS
01
SITE_LOCATION
401 S AIRPORT WAY
P_LOCATION
04
P_DISTRICT
005
QC Status
Approved
Scanner
SJGOV\rtan
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FilePath
\MIGRATIONS\4200 - Liquid Waste\A\AIRPORT WAY\401\PR0526172\MONIT RPTS.PDF
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EHD - Public
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Orenco Systems Inc. March 2002 <br /> AdvanTex AX 10 Test Report <br /> probing revealed that the grey biofilm (in the areas of the filter more distant from the <br /> distribution caps) extended only a few inches below the top of the filter. In contrast, the <br /> black coloured biofilm in the vicinity of the distribution caps extended a greater depth below <br /> the top of the filter. <br /> To improve the liquid distribution across the top of the filter, on April 25, 2001 (Day 192 in <br /> Week 28) the original (35 cap) manifold was replaced with one having a modified <br /> "diamond-shaped" (33 cap) distribution pattern, as illustrated in Photograph #2. The <br /> original filter media below the distribution cap manifold was left in place without any <br /> alteration. The biological build-up on the media was left undisturbed in order to determine <br /> whether the modifications to the distribution pattern would allow the filter to recover from <br /> ` the excessive loading and biofilm condition. <br /> 2.5.3 Increasing the Recirculation Ratio & Media Wetting Frequency <br /> L <br /> During the first 232 days of the test, the flow from the recirculation tank to the filter was set <br /> at one minute of dosing every twenty minutes, achieving a recirculation ratio of 2.0. It was <br /> ✓r noted that the majority of the drainage through the filter media was completed within one <br /> minute of the cessation of dosing, suggesting that the dosing frequency could be increased <br /> Lto improve treatment performance. <br /> On Day 233 in week 34 (June 4), the recirculation flow was changed to 20 seconds every <br /> four minutes. This increased the recirculation ratio to 3.2, and increased the frequency of <br /> ` wetting of the filter media by about five times. Although the process, at this point, had <br /> recovered; the purpose of altering the timer setting was to see if further improvement could <br /> be gained. <br /> 2.5.4 Summary <br /> �- From mid March through the end of April steps were taken to isolate potential causes for <br /> the drop in performance that occurred during the fifth month of testing. Flow to the plant <br /> was kept at 500 gpd throughout this period. The underd rain repair was made first since it <br /> L was physically inhibiting (blocking)discharge from the unit as well as the natural ventilation <br /> through the pod. Effluent quality was monitored closely for about four weeks following the <br /> underdrain repair and little apparent recovery was observed. Next, the manifold <br /> modification was made. Within a couple of weeks the unit had recovered and by the time <br /> the recirculation ratio was increased, the unit was producing an effluent with a CBODS <br /> concentration of under 20 mg/L. <br /> 2.6 Flow Reduction <br /> Prior to repeating the four stress tests in early September, the flow rate was reduced on <br /> August 4, 2001 (at the end of the 42"d week of testing) from 500 to 400 gpd. This was <br /> done to monitor the performance of the unit at a lower hydraulic loading rate. <br /> Nova Tec Consultants Inc. Page 14 of 38 <br />
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