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The reason for this extremely high soil nitrogen content, is due to the fact that the prior land use was <br /> as an agricultural by-product recycler. Mounds of biomass were processed and stored in this area, <br /> thus leaching nitrogen into the soil and groundwater. <br /> Because septic effluent is composed predominately of ammonium(NH4),the pH, along with the CEC, <br /> are significant influences on ammonium molecules. The pH of the soil is slightly alkaline which has a <br /> positive effect in promoting ammonia and not the nitrate substrate ammonium within the soil <br /> environment. <br /> The CEC measures the ability of the soil to theoretically trap and hold ammonium molecules. At 27.3 <br /> meq/100g,the CEC illustrates a very high potential for the clay soil to retain ammonium molecules <br /> that remain as ammonium. Nitrification is also hindered due to the alkaline pH and from the anaerobic <br /> micro-sites within the clay soil. <br /> NLS§3.3, SSS§ 5.3,5.4. Table 1 below summarizes the encountered soil physical and chemical <br /> characteristics: <br /> TABLE 1 <br /> SOIL PROFILE CHARACTERISTICS AND <br /> ANALYTICAL TEST RESULTS <br /> SAMPLE DEPTH AND SOIL SOIL NnRATE-NITROGEN pH AND <br /> (SAMPLE NUNMER ON CLASSIFICATION CONTENT CATION EXCHANGE CAPACITY <br /> -TEST RESULT FORDO) In;meq/100g <br /> BDG24 Silty Clay Loam 189 ppm NO,-N/450 Units 7.3 27.3 me /100g <br /> C. PERCOLATION TEST RESULTS <br /> SSS§ 6.2. To assess the permeability in the 36" boring,which corresponds with the approximate <br /> soil-effluent interface elevation,the aforementioned percolation test borings were completed in the <br /> locations depicted on the Site Plan found in Appendix C. <br /> SSS§ 6.3. After drilling,the sidewalls of the borings were'scored with a pry-bar to open potentially <br /> smeared soil surfaces that may have occurred due to the clay soil,-and the cuttings removed. Two <br /> inches of gravel was placed at the bottom and three-inch perforated PVC pipe was inserted in each <br /> test boring. After these procedures, the borings were pre-saturated with 12 inches of water <br /> approximately 24 hrs prior to the start of testing. <br /> SSS§6.4, 6.5. On February 25, 2019,percolation testing commenced at 0800 hrs. No standing <br /> water was observed after the 24-hr soak period. Consequently, EHD Perc Test Procedure#2 was <br /> conducted. Testing was done over a four-hour period to induce maximum soil saturation,which <br /> was easily achieved since this rainy season was one of the heaviest on record. <br /> Page -3- <br /> Chesney Consulting <br />